Crash of a McDonnell Douglas MD-82 in Surabaya

Date & Time: Mar 4, 2006 at 1625 LT
Type of aircraft:
Operator:
Registration:
PK-LMW
Survivors:
Yes
Schedule:
Denpasar – Surabaya
MSN:
49443/1291
YOM:
1986
Flight number:
JT8987
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
138
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Prior to departure from Bali to Surabaya, the crew was informed that the left engine's thrust reverser system was out of service. Following an uneventful flight, the crew completed a normal approach to runway 10 then landed according to procedures. After touchdown, the crew activated the thrust reverser when the airplane deviated to the right. The crew elected to counteract but the aircraft veered off runway, lost its undercarriage and came to rest in a grassy area. All 144 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a McDonnell Douglas MD-82 in Machiques: 160 killed

Date & Time: Aug 16, 2005 at 0300 LT
Type of aircraft:
Operator:
Registration:
HK-4374X
Flight Phase:
Survivors:
No
Schedule:
Panama City - Fort-de-France
MSN:
49484
YOM:
1986
Flight number:
YH708
Location:
Country:
Crew on board:
8
Crew fatalities:
Pax on board:
152
Pax fatalities:
Other fatalities:
Total fatalities:
160
Captain / Total flying hours:
5942
Captain / Total hours on type:
1128.00
Copilot / Total flying hours:
1341
Copilot / Total hours on type:
862
Aircraft flight hours:
49494
Aircraft flight cycles:
24312
Circumstances:
The MD-82 arrived at Panama City-Tocumen after a flight from Medellín-José María Córdova Airport (MDE). The plane was then prepared to carry out a flight to the Caribbean island of Martinique. Flight WCW 708 departed Panama City at about 06:00 UTC and climbed to its cruising altitude of FL310. This altitude was reached at about 06:25 UTC. Sixteen minutes later the airplane began a normal climb to FL330. At 06:49 the speed began to steadily decrease from Mach 0.76. The horizontal stabilizer moved from about 2 units nose up to about 4 units nose up during this deceleration. At 06:51 UTC the crew reported at FL330 over the SIDOS waypoint, over the Colombian/Venezuelan border, and requested a direct course to the ONGAL waypoint. The controller instructed the crew to continue on the present heading and to await further clearance direct to ONGAL. The flight crew meanwhile discussed weather concerns that included possible icing conditions and the possible need to turn on engine and airfoil anti-ice. At 06:57 UTC the flight crew requested permission to descend to FL310, which was approved. The autopilot was disconnected and the airplane started to descend. As the airplane descended past about FL315, the airspeed continued to decrease and the engine EPR decreased to about flight idle. Two minutes later a further descent to FL290 was requested, but the controller at Maiquetía did not understand that this was a request from flight 708 and asked who was calling. Flight 708 responded and immediately requested descent to FL240. The controller inquired about the state of the aircraft, to which they responded that both engines had flamed out. The controller then cleared the flight to descent at pilot's discretion. In the meantime, the altitude alert warning had activated, followed by the stick shaker and the aural stall warning alert. The airspeed had reached a minimum of about 150 indicated air speed (IAS) knots at about FL250. The crew reported descending through FL140 and reported that they were not able to control the airplane. The aircraft descended at 7,000 ft/min, and finally crashed in a swampy area. The aircraft disintegrated on impact and all 160 occupants were killed. Debris were found on an area of 205 metres long and 110 metres wide. The entire descent from FL330 had taken approximately 3 minutes and 30 seconds.
Probable cause:
Given the aerodynamic and performance conditions, the aircraft was taken to a critical state, which led to a loss of lift. Consequently, the cockpit resource management (CRM) and decision-making during the development of emergency were misguided. This was caused by the following:
a) Awareness of environment (or situational awareness) insufficient or improper that allowed the cockpit crew, not being full and timely aware of what was happening regarding the performance and behavior of the aircraft.
b) Lack of effective communication between the cockpit crew that limited, within the decision making process, the possibility to timely choose appropriate alternatives and options and to set respective priorities in the actions taken at the time when it was established that there was a critical or emergency situation (stall condition at high altitude).
It is found that the cause of the accident is determined by the absence of appropriate action to correct the stall of the aircraft, and also in the emergency up to the impact with the ground, at an inappropriate hierarchy of priorities in implementing the procedures. Subsequently, the operations were conducted outside of the limits and parameters set by the manufacturer's manual performance, together with an inadequate flight planning by failing to consider meteorological aspects, in addition a misinterpretation and late of the energy state of the aircraft by the flight crew. Therefore, the evidence shows the classification of "Human Factor" as a cause of this accident.
Final Report:

Crash of a McDonnell Douglas MD-82 in Surakarta: 25 killed

Date & Time: Nov 30, 2004 at 1815 LT
Type of aircraft:
Operator:
Registration:
PK-LMN
Survivors:
Yes
Schedule:
Jakarta – Surakarta
MSN:
49189
YOM:
1984
Flight number:
JT583
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
156
Pax fatalities:
Other fatalities:
Total fatalities:
25
Aircraft flight hours:
56674
Aircraft flight cycles:
43940
Circumstances:
While descending to Surakarta-Adisumarmo Airport, the crew was informed about stormy conditions at destination with cumulonimbus and heavy rain falls over the airport with a ceiling at 1,500 feet. The approach was continued and after touchdown on runway 26, the crew started the braking procedure and activated the thrust reverser systems. ON a wet runway, the aircraft was unable to stop within the remaining distance. It overran, lost its undercarriage and slid for few dozen metres, collided with equipments of the localizer antenna, a fence and came to rest in a cemetery. Both pilots and 23 passengers were killed while 70 other occupants were injured. 68 occupants escaped unhurt. The aircraft was destroyed.
Probable cause:
The following findings were identified:
- About 3 mm of water was stagnating on the runway surface, reducing the braking action,
- The crew completed the landing procedure with a 13 knots tailwind component,
- Airbrakes deployed after touchdown but retracted few seconds later due to wrong position of the power levers,
- Power levers were not in idle position after touchdown but slightly forward, so the flight computer increased power,
- Heavy rain falls,
- The crew failed to initiate a go-around procedure.