Crash of a Lockheed L-188C Electra in Manado: 22 killed

Date & Time: Feb 16, 1967 at 1321 LT
Type of aircraft:
Operator:
Registration:
PK-GLB
Survivors:
Yes
Schedule:
Jakarta – Surabaya – Ujung Pandang – Manado
MSN:
2021
YOM:
1960
Flight number:
GA708
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
84
Pax fatalities:
Other fatalities:
Total fatalities:
22
Captain / Total flying hours:
8054
Captain / Total hours on type:
718.00
Copilot / Total flying hours:
8336
Copilot / Total hours on type:
505
Aircraft flight hours:
12359
Circumstances:
Flight 708 was a scheduled domestic flight from Jakarta to Manado, with intermediate stops at Surabaya and Makassar. It departed Djakarta at 0030 hours GMT on 15 February and proceeded on an IFR flight plan to Surabaya. While en route to Surabaya No. 4 engine would not synchronize. The flight landed at 0200 hours at Surabaya where an oil leak on No. 1 propeller was found. After rectifying these faults the flight departed from Surabaya at 0300 hours. On approaching Makassar bad weather was reported and after two attempts to land, the pilot-in-command elected to divert to another aerodrome. Two aerodromes were available - Denpasar, the first alternate and Surabaya. Although Surabaya was at a greater distance, the pilot-in-command decided for various reasons to return to Surabaya-Juanda and remain overnight. An oil leak on No. 1 propeller was again observed and noted for rectification. The flight departed the next morning at 0010 hours for Makassar where it landed without incident. After approximately a one hour stop at Makassar the flight proceeded to Menado with an estimated time of arrival there of 0512 hours GMT. On approaching Menado the pilot-in-command requested the weather conditions and was given a cloud base of 900 ft and a visibility of 2 km. At an altitude of 1 500 ft the town of Menado and the beach were visible and the aircraft made a 360° turn over the bay of Menado: the aircraft then descended to 900 ft and intercepted the beach on a heading of 120' intending to make an approach to runway 18. The pilot-in-command sighted the runway to his right, continued the approach through a gap between two hills, and called for the undercarriage to be lowered and completion of final checks. He instructed the flight engineer to stand by for an overshoot at which time the approach was being continued with the flaps in the landing position. The aircraft banked 15°-20° to the right, and the co-pilot monitored and called the airspeed. After passing a hill 200 ft above the runway elevation and some 2 720 ft before the runway threshold the pilot-in-command realized he was too high, also the aircraft was still to the left of the centre line and banked to the right. The nose of the aircraft was lowered and after intercepting the glide path at an indicated airspeed of 130 kt the control column was moved rearwards to a normal descent position. With the airspeed rapidly decreasing below the target threshold speed of 125 kt, and whilst still banked to the right, the aircraft landed heavily 3 ft short of the runway manoeuvring area and some 156 ft short of the runway threshold. The undercarriage collapsed and the aircraft skidded, caught fire and came to rest on the runway 1 442 ft after the threshold on a heading of 225°. 22 passengers were killed.
Probable cause:
The Board determined that the probable cause of this accident was an awkward approach technique resulting in an excessive rate of sink on touchdown. Based on all available evidence the Board found that the following factors contributed to the accident:
- The runway width of 98 ft which looks smaller from the pilot's point of view,
- The uneven runway pavement which forces pilots to touchdown as close as possible to the threshold,
- The marginal weather conditions prevailing at the time of the accident which forced the pilot to accomplish a tight circuit,
- The relationship between the rate of sink and the negative thrust at low speed were not known to the pilot and the operator.
Final Report:

Crash of a Lockheed L-188C Electra in Ardmore: 83 killed

Date & Time: Apr 22, 1966 at 2030 LT
Type of aircraft:
Operator:
Registration:
N183H
Survivors:
Yes
Schedule:
Monterey - Ardmore - Columbus
MSN:
1136
YOM:
1961
Flight number:
AFA280D
Crew on board:
5
Crew fatalities:
Pax on board:
93
Pax fatalities:
Other fatalities:
Total fatalities:
83
Captain / Total flying hours:
16247
Captain / Total hours on type:
1247.00
Copilot / Total flying hours:
12355
Copilot / Total hours on type:
1155
Aircraft flight hours:
4019
Circumstances:
The aircraft departed Monterey Airport, California, on a charter flight to Columbus, Georgia, with an intermediate stop at Ardmore Municipal Airport, Oklahoma, carrying 93 US soldiers and a crew of five on behalf of the Military Air Command. Following an uneventful flight from Monterey, the crew started the descent to Ardmore Municipal Airport by night and marginal weather conditions. An ADF instrument approach to runway 08 was abandoned and the crew decided to follow a visual approach to runway 30. While descending to runway 30 in poor visibility, the captain (also PIC) suffered a heart attack. The aircraft commenced an uncontrolled descent slightly banked to the right until it struck the ground and disintegrated about 1,5 mile short of runway 30. All five crew members and 75 passengers were killed while 18 others were seriously injured. Few hours later, three of the survivors died from their injuries.
Probable cause:
The Board determined the probable cause of this accident was the incapacitation, due to a coronary insufficiency, of the pilot-in-command at a critical point during visual, circling approach being conducted under instrument flight conditions. The Board was concerned by the fact that the pilot-in-command has an established medical history of cardiovascular disease and diabetes mellitus, both of which are disqualifying for the issuance of a first-class medical certificate, and that he deliberately falsified his application for this certificate.
Final Report:

Crash of a Lockheed L-188C Electra in Whenuapai

Date & Time: Mar 27, 1965
Type of aircraft:
Operator:
Registration:
ZK-TEC
Flight Type:
Survivors:
Yes
Schedule:
Whenuapai - Whenuapai
MSN:
2011
YOM:
1959
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training mission at Whenuapai Airport. Following several uneventful manoeuvres, the crew completed a new approach for landing when, on short final, the airplane sank and stuck the runway surface at a speed of 140 knots. On impact, the left main gear was sheared off and the airplane went out of control and veered off runway to the left. While contacting soft ground, the left wing was torn off and the aircraft came to rest in flames. All six occupants were evacuated safely while the aircraft was destroyed.
Probable cause:
It is believed that control was lost between the last segment and flare due to a wrong approach configuration.

Crash of a Lockheed L-188A Electra in Knoxville

Date & Time: Aug 6, 1962 at 1731 LT
Type of aircraft:
Operator:
Registration:
N6102A
Survivors:
Yes
Schedule:
Dallas – Little Rock – Memphis – Knoxville – Washington DC – New York
MSN:
1019
YOM:
1958
Flight number:
AA414
Crew on board:
5
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20634
Captain / Total hours on type:
878.00
Copilot / Total flying hours:
11000
Copilot / Total hours on type:
423
Aircraft flight hours:
6947
Circumstances:
On August 6, 1962, at 1731 e.s.t., Flight 414, an American Airlines, Inc., Lockhead Electra, N 6102A, crashed during a landing on runway 4L at McGhee-Tyson Airport, Knoxville, Tennessee. Sixty-seven passengers and five crew members were on board the aircraft. All escaped injury except one passenger who suffered a minor injury. The aircraft was substantially damaged. During the landing made by the captain in an area of thunderstorm activity and heavy rain showers, the aircraft skidded to the right off the runway. It struck a newly constructed taxiway the surface of which was approximately 17 inches above ground level, causing failure of the right main landing gear. The right wing became separated front the aircraft. The remainder of the aircraft continued to deviate to the right off the side of the runway for a short distance and came to rest 3,010 feet from the approach end of the runway on a heading of 200 degrees magnetic.
Probable cause:
The Board determines that the probable cause of this accident was the loss of directional control as a result of the improper technique employed in a crosswind landing in adverse weather conditions.
Final Report:

Crash of a Lockheed L-188C Electra in Chicago: 37 killed

Date & Time: Sep 17, 1961 at 0857 LT
Type of aircraft:
Operator:
Registration:
N137US
Flight Phase:
Survivors:
No
Schedule:
Milwaukee – Chicago – Tampa – Fort Lauderdale – Miami
MSN:
1142
YOM:
1961
Flight number:
NW706
Crew on board:
5
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
37
Captain / Total flying hours:
15898
Captain / Total hours on type:
314.00
Copilot / Total flying hours:
6643
Copilot / Total hours on type:
90
Aircraft flight hours:
614
Circumstances:
At approximately 0855 1, the flight was cleared for takeoff on runway 14R. At this time the aircraft was taxing on a westerly heading in the runup area adjacent to runway 14R. Flight 706 acknowledged the clearance, while continuing toward the runway, and made a running takeoff No witnesses were found who observed the actual lift-off. N137US was observed after lift-off, 3,000 to 4,000 feet down the runway at an estimated altitude of 50 to 75 feet and in a normal climb attitude. At the 8,000-foot marker the altitude of the aircraft was estimated to have been approximately 100 feet, which is a slightly lower altitude than Electra aircraft normally attain at this point during takeoff. Five witnesses noted a change in engine sound during this portion of the flight. Between the 8,000 and the 9,000 foot runway marker the aircraft was observed to commence an apparently coordinated right turn with a slowly increasing rate of bank. When the bank angle was 30 to 45 degrees, the crew made a short, garbled transmission. Immediately thereafter, at a bank angle of 50 to 60 degrees, the aircraft began to lose altitude. The minimum altitude attained in the entire turn was 200 to 300 feet. The right wing near the No. 4 engine struck powerlines adjacent to the Chicago Northwestern Railroad tracks, severing the lines at an angle of about 70 degrees from the horizontal, and causing a bright bluish flash. The aircraft then continued in a direction of about 271 degrees magnetic and, when in a bank of about 85 degrees and a nose-down attitude of about 10 degrees, the right wing of the aircraft struck the railroad embankment. Continuing to roll about its longitudinal axis, the aircraft cartwheeled, the nose crashing into the ground 380 feet beyond the point of first Impact, and landed right side up It then slid tall first another 820 feet. The aircraft disintegrated throughout its path, and wreckage was strewn over an area 200 feet wide and 1,200 feet long. Evidence of ground fire was found at various points along this path. Impact occurred on airport property about 3,800 feet abeam and to the right of the end of runway 14R, about 500 feet north of Irving Park Road. After passing beyond the railroad embankment the aircraft was lost to view by most of the eye witnesses because of trees and other obstructions; immediately thereafter a large mushroom of orange-red flame accompanied by heavy black smoke was seen. Time of impact was established as 0857. The aircraft was demolished by impact and fire. All occupants were fatally injured.
Probable cause:
The Board determines that the probable cause of this accident was a mechanical failure in the aileron primary control system due to an improper replacement of the aileron boost assembly, resulting in a loss of lateral control of the aircraft at an altitude too low to effect recovery.
Final Report:

Crash of a Lockheed L-188C Electra in Cairo: 20 killed

Date & Time: Jun 12, 1961 at 0411 LT
Type of aircraft:
Operator:
Registration:
PH-LLM
Survivors:
Yes
Schedule:
Amsterdam – Munich – Rome – Cairo – Karachi – Kuala Lumpur
MSN:
2019
YOM:
1960
Flight number:
KL823
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
20
Captain / Total flying hours:
11489
Captain / Total hours on type:
100.00
Copilot / Total flying hours:
3821
Copilot / Total hours on type:
747
Circumstances:
The approach to Cairo-Intl Airport was completed by night. On final, the four engine aircraft struck a hill and crashed 4 km short of runway 34 threshold. Three crew members and 17 passengers were killed while 16 other occupants were injured. The aircraft was destroyed. Following a crew error, the aircraft was below the glide.
Probable cause:
The accident was caused by the pilot-in-command inattention to his instruments.
Final Report:

Crash of a Lockheed L-188A Electra in Boston: 62 killed

Date & Time: Oct 4, 1960 at 1740 LT
Type of aircraft:
Operator:
Registration:
N5533
Flight Phase:
Survivors:
Yes
Schedule:
Boston – Philadelphia – Atlanta
MSN:
1062
YOM:
1959
Flight number:
EA375
Crew on board:
5
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
62
Captain / Total flying hours:
23195
Captain / Total hours on type:
1053.00
Copilot / Total flying hours:
5820
Copilot / Total hours on type:
201
Aircraft flight hours:
3526
Circumstances:
On October 4, 1960, at 1740 e.d.t., an Eastern Air Lines Lockheed Electra, N 5533, crashed into Winthrop Bay immediately following takeoff from runway 9 at Logan International Airport, Boston, Massachusetts. Ten of the 72 persons aboard survived the crash. The aircraft was totally destroyed. A few seconds after becoming airborne, the aircraft struck a flock of starlings. A number of these birds were ingested In engines Nos. 1, 2, and 4. Engine No. 1 was shut down and its propeller was feathered. Nos. 2 and 4 experienced a substantial momentary loss of power. This abrupt and intermittent loss and recovery of power resulted in the aircraft yawing to the left and decelerating to the stall speed. As speed decayed during the continued yaw and skidding left turn, the stall speed was reached; the left wing dropped, the nose pitched up, and the aircraft rolled left into a spin and fell almost vertically into the water. An altitude of less than 150 feet precluded recovery. The Board determines that the probable cause of this accident was the unique and critical sequence of the loss and recovery of engine power following bird ingestion, resulting in loss of airspeed and control during takeoff.
Probable cause:
The Board determines that the probable cause of this accident was the unique and critical sequence of the loss and recovery of engine power following bird ingestion, resulting in loss of airspeed and control during takeoff.
Final Report:

Crash of a Lockheed L-188A Electra in LaGuardia

Date & Time: Sep 14, 1960 at 0800 LT
Type of aircraft:
Operator:
Registration:
N6127A
Survivors:
Yes
Schedule:
Boston – New York – Saint Louis
MSN:
1117
YOM:
1960
Flight number:
AA361
Crew on board:
6
Crew fatalities:
Pax on board:
70
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14082
Captain / Total hours on type:
279.00
Copilot / Total flying hours:
18310
Copilot / Total hours on type:
460
Aircraft flight hours:
1573
Circumstances:
The Electra scheduled as Flight 361 departed Boston at 0716LT with its destination St Louis, Missouri, and with a planned intermediate stop at LaGuardia Airport. About ten minutes prior to departure a crew change was made when a check pilot boarded the aircraft to flight-check the flight engineer. This check pilot, by mutual agreement with the crew and in accordance with existing company policy, took over the left or pilot-in-command seat with the previously assigned captain moving to the jump seat. The trip was routine until final approach at LaGuardia. On final approach, the airplane aircraft was too low and struck a dyke with its main landing gear and crash landed. Approximately half of the 76 persons on board suffered minor injuries or shock; no one was killed. The aircraft was severely damaged by impact forces and fire.
Probable cause:
The Board determines that the probable cause of this accident was the failure of the pilot to properly plan and execute the approach to a landing. Factors which may have contributed were the shortened runway and the unmarked upper portion of the dike.
Final Report:

Crash of a Lockheed L-188C Electra near Tell City: 63 killed

Date & Time: Mar 17, 1960 at 1525 LT
Type of aircraft:
Operator:
Registration:
N121US
Flight Phase:
Survivors:
No
Schedule:
Minneapolis – Chicago – Miami
MSN:
1057
YOM:
1959
Flight number:
NW710
Crew on board:
6
Crew fatalities:
Pax on board:
57
Pax fatalities:
Other fatalities:
Total fatalities:
63
Captain / Total flying hours:
27523
Captain / Total hours on type:
254.00
Copilot / Total flying hours:
2974
Copilot / Total hours on type:
200
Aircraft flight hours:
1786
Circumstances:
The four engine aircraft departed Chicago-Midway at 1438LT bound for Miami, carrying 57 passengers and a crew of six. While cruising at an altitude of 18,000 feet over the south of Indiana State, the aircraft entered a dive and crashed in a huge explosion in a snow covered field located east of Tell City. Some debris were also found in a wooded area. The aircraft disintegrated on impact and all 63 occupants were killed. The crew was unable to send any distress call prior to the accident.
Probable cause:
The Board determines that the probable cause of this accident was the separation of the right wing in flight due to flutter induced by oscillations of the outboard nacelles. Contributing factors were a reduced stiffness of the structure and the entry of the aircraft into an area of severe clear air turbulence.
Final Report:

Crash of a Lockheed L-188A Electra near Buffalo: 34 killed

Date & Time: Sep 29, 1959 at 2309 LT
Type of aircraft:
Operator:
Registration:
N9705C
Flight Phase:
Survivors:
No
Schedule:
Houston – Dallas – Washington DC – New York
MSN:
1090
YOM:
1959
Flight number:
BN542
Location:
Crew on board:
6
Crew fatalities:
Pax on board:
28
Pax fatalities:
Other fatalities:
Total fatalities:
34
Captain / Total flying hours:
20726
Captain / Total hours on type:
68.00
Copilot / Total flying hours:
11316
Copilot / Total hours on type:
95
Aircraft flight hours:
132
Circumstances:
Flight 542 departed the ramp at Houston at 2237LT, 22 minutes behind schedule with a total of 34 persons including a crew of six consisting of Captain Wilson Elza Stone, First Officer Dan Hollowell, Second Officer Roland Longhill, and Stewardesses Alvilyn Harrison, Betty Rusch and Leona Winkler, none of whom survived. The delayed departure was due to a mechanical discrepancy involving No. 3 generator. This generator was inoperative on arrival of N9705C at Houston. Prior to departure from Houston the Nos. 3 and 4 voltage regulators were interchanged. Actual gross weight upon departure was calculated at 83,252 pounds, including 17,000 pounds of fuel, and was 16,548 pounds less than the authorized gross weight of 99,800 pounds. The estimated time en route to Dallas was 41 minutes. The flight was given an instrument-flight-rules clearance which was to the Leona omni, via Victor Airway 13 west to the Gulf Coast intersection, direct to Leona, to maintain 2,300 feet altitude to Gulf Coast, then to climb to and maintain 9,000. At approximately 2240 the flight was cleared for takeoff and at 2242 it reported ready for takeoff and was airborne at 2244. After takeoff Houston departure control advised that it had the flight in radar contact and requested it to report when established outbound on the 345-degree radial of the Houston omni. Flight 542 complied and subsequently was cleared to 9,000 feet and advised to contact San Antonio Center on 121.1 mcs. upon passing the Gulf Coast intersection. Flight 542 reported to company radio at 2251 as blocking out of Houston at 37, taking off at 42, to cruise at 15,000 feet when so cleared, estimating Dallas at 2325, and that the Center had this information. At approximately 2252 Flight 542 reported to San Antonio Center as being over Gulf Coast intersection at 9,000 feet. The flight was then issued its destination clearance to the Dallas Airport via direct to Leona, direct to Trinidad, direct to Forney, direct to Dallas, to maintain 15,000 feet. The flight was cleared to climb to its cruising altitude. The next transmission from Flight 542 was to the San Antonio, Center, giving the time over Leona as 05 at 15,000. San Antonio Center acknowledged, and requested Flight 542 to change over and monitor the Fort Worth frequency of 120.8 mcs. at this time. The flight acknowledged. Shortly thereafter Flight 542 contacted company radio with a message for maintenance, advising that the generators were then OK out that there had been insufficient time for maintenance to insulate the terminal strip on No. 3 propeller at Houston and it would like to have it done in Dallas. At this time the flight also said it would give the communication center a Dallas estimate of 25. This was then followed by one other item for maintenance, which was that No. 3 sump pump was inoperative. This was the final transmission from the flight and was logged as completed at 2307. Structural failure of the aircraft occurred at approximately 2309 on course to the next fix, Trinidad intersection. The radial from Leona omni to Trinidad intersection is 344 degrees. The main wreckage was located 19.7 miles 2 north of Leona omni, 3.19 miles east-southeast of Buffalo, Texas. The time, 2309, correlates closely with the information obtained from witnesses to the accident as well as the time indicated on impact-stopped watches recovered at the scene. The aircraft was destroyed upon impact and all 34 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was structural failure of the left wing resulting from forces generated by undampened propeller whirl mode.
Final Report: