Crash of a Piper PA-31T3-T1040 Cheyenne in Atlanta

Date & Time: Sep 24, 1984 at 1609 LT
Type of aircraft:
Registration:
N9193Y
Survivors:
Yes
Schedule:
Florence - Atlanta
MSN:
31T-8275010
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3309
Captain / Total hours on type:
439.00
Aircraft flight hours:
1857
Circumstances:
The normal fuel load for the flight was 1,500 lbs, but with a forecast tail wind and an estimated flight time for only 1+10, the crew accepted the lower indicated (950 lb) fuel load. The flight was uneventful until an indication of 250 lbs per side, then the fuel 'seemed to dissipate faster.' With an indication of 150 lbs on downwind, the copilot recommended declaring an emergency. The captain's response was to ask ATC for the anticipated length of the downwind leg. He was told 20 miles. Priority handling was requested, but was only available for a declared emergency. The approach was continued with normal handling for approximately 10 minutes. At 1608:39, the crew declared an emergency, then reported the aircraft was out of fuel. It crash landed on rough terrain, short of runway 08. An exam revealed fuel sensors had been improperly installed (interchanged between the inboard and outboard tanks). Thus the gages indicated about 180 lbs more than the approximately 763 lbs that was actually aboard at takeoff. A special 500 hour inspection of the entire fuel system was made on 7/8/84 using the 'wet' method, but only the capacitance method checks each individual sensor. All 11 occupants were injured and the aircraft was destroyed.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) fuel system - incorrect
2. (f) maintenance, installation - improper
3. (f) engine instruments, fuel quantity gage - false indication
4. Maintenance, inspection - inadequate
5. (f) procedure inadequate - manufacturer
6. (f) fluid, fuel - low level
7. (c) in-flight planning/decision - improper - pilot in command
8. (c) remedial action - delayed - pilot in command
9. (c) fluid, fuel - exhaustion
10. Fuel supply - inadequate
----------
Occurrence #2: forced landing
Phase of operation: approach - faf/outer marker to threshold (ifr)
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
Findings
11. (f) terrain condition - rough/uneven
Final Report:

Crash of a Cessna 421C Golden Eagle III in Kennesaw: 4 killed

Date & Time: Aug 8, 1984 at 0732 LT
Operator:
Registration:
N98457
Flight Phase:
Survivors:
No
MSN:
421C-0050
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
869
Captain / Total hours on type:
11.00
Circumstances:
According to witnesses, the aircraft entered clouds at low altitude during the initial climb after takeoff. They reported that the aircraft then turned sharply back toward the airport and descended below the clouds. It rolled out in the direction of the crash site with the wings rocking. One witness said the aircraft 'turned over 2 or 3 times' before it crashed. No preimpact part failure or malfunction was evident. All four occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: takeoff - initial climb
Findings
1. (c) preflight planning/preparation - inadequate - pilot in command
2. (f) weather condition - low ceiling
3. (f) weather condition - fog
4. (c) vfr flight into imc - inadvertent - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: maneuvering - turn to reverse direction
Findings
5. Maneuver - initiated - pilot in command
6. (c) airspeed - not maintained - pilot in command
7. Stall/spin - uncontrolled - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent – uncontrolled
Final Report:

Crash of a Beechcraft U-8F Seminole in Hiram: 3 killed

Date & Time: Oct 19, 1983 at 1300 LT
Type of aircraft:
Operator:
Registration:
62-3839
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Dobbins - Dobbins
MSN:
LF-37
YOM:
1962
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
6000
Copilot / Total flying hours:
5200
Circumstances:
The twin engine airplane departed Dobbins AFB on a local training flight, carrying two pilots and one instructor. While flying at an altitude between 1,900 and 2,100 feet, the crew reduced the speed, lower the gears and the flaps then initiated a 180 turn when control was lost. The aircraft entered a dive and crashed in a wooded area located in Hiram, bursting into flames. All three occupants were killed.
Crew:
Cw2 James Q. Tyner Jr.,
Civ John R. Bailey,
Maj David M. Bishop.

Crash of a Beechcraft 65-A80 Queen Air in Edison

Date & Time: Oct 12, 1983 at 2130 LT
Type of aircraft:
Operator:
Registration:
N62TG
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
LD-215
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At approximately 2130 edt, the aircraft collided with a tree while the pilot was making a low pass over a wooded area. After hitting the tree, the plane crashed into a pond. Reportedly, the aircraft had returned from Columbia (South America) and the aircrew were preparing to drop duffel bags of cocaine. When the aircraft hit the tree, the pilot was flying while the other person was getting ready to throw out the bags. Both occupants were seriously injured.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: maneuvering
Findings
1. (f) light condition - night
2. (c) judgment - poor - pilot in command
3. (f) overconfidence in personal ability - pilot in command
4. (f) low pass - performed - pilot in command
5. (c) proper altitude - not maintained - pilot in command
6. (f) object - tree(s)
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Lockheed 18 LodeStar in Millhaven: 2 killed

Date & Time: Jun 23, 1983 at 0157 LT
Type of aircraft:
Registration:
N333FB
Flight Type:
Survivors:
No
MSN:
2467
YOM:
1957
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The aircraft collided with trees during an attempted off airport landing at night for marijuana unloading. The aircraft was being followed by a u.s customs helicopter, the occupants of this helicopter said the aircraft had made one missed approach and during the go-around on the downwind leg the aircraft descended until it hit the trees. There was a layer of 'scud' at about 100-200 feet agl. Visibility under the low lying intermittent cloud layer was about 2 miles. After the crash the helicopter landed about 30 yards away but approach on foot was not possible due to heat from the burning wreckage. Both occupants were killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - VFR pattern - downwind
Findings
1. (c) altitude - not maintained - pilot in command
2. (c) diverted attention - pilot in command
3. (f) weather condition - fog
4. (f) light condition - dark night
5. (f) object - tree(s)
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise in Jeffersonville: 4 killed

Date & Time: Mar 24, 1983 at 0236 LT
Type of aircraft:
Registration:
N72B
Flight Phase:
Survivors:
No
Schedule:
Jacksonville - Atlanta
MSN:
735
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3747
Captain / Total hours on type:
547.00
Circumstances:
The aircraft was on the return portion of a round trip flight, hauling canceled bank checks. When they boarded before takeoff, the pilot's wife, who was not a pilot, occupied the right front seat and his two daughter's, ages 4 and 6, were in the passenger seats. Previous legs of the flight were accomplished without incident. While en route on the 4th leg, a radar handoff was made from Jacksonville to Atlanta Center at 0225 est and the pilot reported at FL180. This was his last known transmission. At 0230, the ATC controller noted the aircraft was passing Macon VOR. Shortly thereafter, radar contact was lost and efforts to make radio contact were unsuccessful. Several persons in the vicinity heard the aircraft engines alternately at high speed, then demishing, before the accident. The wreckage was found scattered over a 2 miles area. An exam revealed the right wing had failed upward and the left wing and left horizontal stabilizer had failed downward from overload. There was evidence of course reversal and descent before breakup; light turbulence and icing at cruise alt. Reason for descent unknown. All four occupants were killed.
Probable cause:
The uncontrolled descent of the airplane for undetermined reasons and the overstress and breakup of the airplane structure during an attempted recovery by the pilot.
Final Report:

Crash of a Lockheed 18-56 LodeStar in Madison

Date & Time: Jan 11, 1983 at 1450 LT
Type of aircraft:
Registration:
N520R
Flight Phase:
Survivors:
Yes
Schedule:
Madison - Miami
MSN:
2183
YOM:
1941
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15245
Captain / Total hours on type:
28.00
Aircraft flight hours:
10823
Circumstances:
The pilot reported that after he taxied to the rwy, the n°1 oil temperature was not up to the minimum temperature. He set the parking and advanced the n°1 throttle to 1,500 rpm until the engine warmed up. When both oil temperatures were within limits, he advanced both throttles to 30 inches manifold pressure and 2,250 rpm for a pretakeoff check. At that time, he used the normal (toe) brakes, since the parking brake would not hold the aircraft above approximately 1,700 rpm. He then applied full power and released the brakes for takeoff. As he started to roll with a slight left crosswind, the aircraft began drifting left. He corrected with right rudder, some right brake and right aileron. The aircraft then began drifting right and the pilot suspected a wind-shift from that direction. He applied left rudder and right aileron, but the plane veered right, went off the runway and headed for a ditch. Unable to stop, the pilot tried to clear the ditch. As the aircraft became airborne, the left wing dropped and hit the ground, and the aircraft yawed and crashed. The parking brake was found partially engaged. Tire marks were evident on the runway. All four occupants escaped uninjured.
Probable cause:
Occurrence #1: loss of control - on ground/water
Phase of operation: takeoff - roll/run
Findings
1. (c) parking brakes - inadvertent use - pilot in command
2. (f) lack of total experience in type of aircraft - pilot in command
3. (f) weather condition - crosswind
4. (f) directional control - not maintained - pilot in command
5. (f) ground loop/swerve - uncontrolled - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff
Findings
6. (f) terrain condition - ditch
7. (f) lift-off - initiated - pilot in command
8. (f) stall/mush
Final Report:

Crash of a Cessna 421B Golden Eagle II in Savannah: 4 killed

Date & Time: Dec 11, 1982 at 0025 LT
Operator:
Registration:
N8001Q
Survivors:
No
Schedule:
Charleston - Savannah
MSN:
421B-0001
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3300
Circumstances:
The pilot reported he was on a missed approach and was returning to Charleston "heading 360°..." the aircraft crashed about 1/4 mi south and 100 feet short of the departure end of runway 27. The wreckage scatter pattern was oriented on a heading of 155°. Missed approach procedures specify a climbing right turn via a 325° heading. The left engine prop drive gear shaft had evidence of both bending and torsional failure loads. There was no evidence of machining or rotational smearing. Two of the three propeller blade tips were bent aft about the blade face. The left turbocharger had a tension failure of the turbine wheel shaft. No smear marks were noted on the fracture face. Single turbine blade impact marks were noted on the housing. The n°1 tach needle indicated 900 rpm and the n°2 tach needle indicated 1,900 rpm. All four occupants were killed.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: missed approach (IFR)
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: loss of control - in flight
Phase of operation: missed approach (IFR)
Findings
2. (f) light condition - dark night
3. (f) weather condition - low ceiling
4. (f) weather condition - fog
5. (f) weather condition - below approach/landing minimums
6. (f) missed approach - performed - pilot in command
7. (c) aircraft handling - not possible - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: missed approach (IFR)
Final Report:

Crash of a Rockwell 680W Turbo II Commander in Atlanta

Date & Time: Nov 20, 1982 at 1930 LT
Operator:
Registration:
N5058E
Flight Type:
Survivors:
Yes
Schedule:
Charlotte - Atlanta
MSN:
680-1787-17
YOM:
1968
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3420
Captain / Total hours on type:
143.00
Aircraft flight hours:
2306
Circumstances:
The pilot reported that on the previous flight, the center fuel tank gauge was malfunctioning and indicated 800 lbs even when it was full with 1400 lbs. After landing at Charlotte, NC, it was still indicating 800 lbs. Before takeoff, the center tank was refilled. While en route about 40 miles west of Atlanta, GA, the pilot noted that the fuel gauge indicated 500 lbs and was dropping rapidly. A few minutes later, both engines flamed out. Vectors were obtained to fly to the nearest airport. During the descent, the engines were restarted. The pilot intercepted the ILS and remained high on the glide slope. The weather at the airport was reported as 100 feet overcast, visibility 1/4 mile with fog and rain. The aircraft broke out of the clouds approximately 2/3 of the way down the runway, then continued off the end of the runway and went thru ILS antenna array. An exam revealed the center fuel cap was missing, it was found in the grass near the parking ramp at Charlotte. The fuel cap was found to be worn and would not lock securely.
Probable cause:
Occurrence #1: loss of engine power(total) - non mechanical
Phase of operation: cruise - normal
Findings
1. (f) engine instruments,fuel quantity gauge - incorrect
2. (f) operation with known deficiencies in equipment - performed - pilot in command
3. (c) fuel system,cap - worn
4. (c) fuel system,cap - separation
5. (c) fluid,fuel - loss,partial
6. (c) fluid,fuel - starvation
7. Aircraft performance,two or more engines - inoperative
----------
Occurrence #2: overrun
Phase of operation: landing - roll
Findings
8. Emergency procedure - performed - pilot in command
9. Precautionary landing - performed - pilot in command
10. (f) weather condition - low ceiling
11. (f) weather condition - fog
----------
Occurrence #3: on ground/water collision with object
Phase of operation: landing - roll
Findings
12. (f) object - approach light/navaid
Final Report:

Crash of a Learjet 23 off Savannah: 4 killed

Date & Time: May 6, 1982 at 1200 LT
Type of aircraft:
Registration:
N100TA
Flight Phase:
Survivors:
No
Schedule:
Teterboro - Orlando
MSN:
23-045
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
7000
Captain / Total hours on type:
150.00
Copilot / Total flying hours:
1550
Copilot / Total hours on type:
125
Aircraft flight hours:
7100
Circumstances:
While in cruise flight on Airway J79-121 en route to Orlando, Florida, from Teterboro, New Jersey, the flightcrew of N100TA, an IBEX Corporation Gates Learjet 23, was cleared by the Jacksonville Air Route Traffic Control Center to descend from its altitude of Flight Level 410 to Flight Level 390. The flightcrew acknowledged the clearance, and air traffic control observed the radar target descend. About 2 minutes later, the airplane crashed into the Atlantic Ocean, from a steep, high-speed descent about 12 miles from Savannah, Georgia. The air traffic controller made several unsuccessful attempts to contact the airplane. The pilots had reported no difficulties in any of their radio transmissions. The pilot, copilot, and the two passengers on board were killed. Beyond 1158:49, the program showed a gradual increase in indicated airspeed from 271 to 400 KIAS. The average rate of descent was 15,375 fpm based on the radar data using pressure altitude (mode C).
Probable cause:
The National Transportation Safety Board determines that the probable cause of the accident was an uncontrolled descent from cruise altitude for undetermined reasons, from which a recovery was not or could not be effected.
Final Report: