Crash of a Beechcraft C18S Expeditor on Wassaw Island: 2 killed

Date & Time: Jul 4, 1980 at 0930 LT
Type of aircraft:
Registration:
N35MS
Flight Phase:
Survivors:
No
Schedule:
Charleston - Kings Bay
MSN:
6947
YOM:
1944
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8000
Circumstances:
The crew departed Charleston-Executive Airport (Johns Island) in the morning on a flight to Kings Bay, Georgia, taking part to a mosquito control mission. En route, the twin engine airplane went out of control, dove into the ground and crashed in a wooded area located on Wassaw Island. The aircraft caught fire on impact and both occupants were killed.
Probable cause:
Uncontrolled descent due to crew incapacitation. The aircraft was observed in shallow descent til impact. Dibrom 14 on board produces blinding fumes if atomized. Liquid chemical toxic.
Final Report:

Crash of a Beechcraft 65 Queen Air in Kennesaw

Date & Time: Jul 2, 1980 at 0839 LT
Type of aircraft:
Operator:
Registration:
N22PC
Flight Type:
Survivors:
Yes
Schedule:
Kennesaw – Atlanta – Fort Lauderdale
MSN:
LC-69
YOM:
1961
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
803
Captain / Total hours on type:
20.00
Circumstances:
Few minutes after takeoff from Kennesaw-McCollum Airport, the pilot encountered technical problems and elected to return. On final approach, he decided to initiate a go-around when the airplane stalled, crashed and burst into flames. The pilot was seriously injured.
Probable cause:
Engine malfunction during climb to cruise and subsequent stall and crash on go-around due to improper operation of powerplant and powerplant controls on part of the pilot. The following contributing factors were reported :
- Detonation in powerplant,
- Cooling system: cowling, deteriorated,
- The pilot failed to maintain flying speed,
- Inadequate preflight preparation,
- Lack of familiarity with aircraft,
- Complete engine failure of the right engine,
- Right side of right engine cowling seals destroyed,
- Battery not installed in aircraft.
Final Report:

Crash of a Sud-Aviation SE-210 Caravelle VI-R in Atlanta

Date & Time: Jun 19, 1980 at 0456 LT
Operator:
Registration:
N905MW
Flight Type:
Survivors:
Yes
Schedule:
San Jose - Wilmington - Atlanta
MSN:
95
YOM:
1961
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9941
Captain / Total hours on type:
1239.00
Circumstances:
The crew was completing a night cargo flight from San Jose, California, to Atlanta with intermediate stop in Wilmington, Ohio. On approach, the airplane became unstable and rolled left and right. Despite the situation, the crew decided to continue the approach to runway 26 when the airplane landed hard. Upon touchdown, the left main gear collapsed. The airplane rolled for about 4,526 feet then veered off runway to the left and came to rest 250 feet further in a grassy area. All four occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Hard landing and subsequent failure of the left main gear after the crew failed to follow approved procedures. The following contributing factors were reported:
- Poorly planned approach,
- Vortex turbulences,
- Fast from LOM to airport,
- Closed gap behind a Lockheed L-1011 Tristar that just landed on same runway.
Final Report:

Crash of a Lockheed 18-56-23 LodeStar in Brunswick

Date & Time: Jul 24, 1979 at 1600 LT
Type of aircraft:
Registration:
N33LM
Flight Type:
Survivors:
Yes
Schedule:
Rockmart - Brunswick
MSN:
2341
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11500
Captain / Total hours on type:
85.00
Circumstances:
Upon landing at Brunswick-Glynco Jetport Airport, the twin engine airplane bounced. The gear collapsed and the airplane went out of control and came to rest on its belly. All three occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Ground loop/swerve and subsequent gear collapsed upon landing due to improper recovery from bounced landing and improper operation of brakes and flight controls. The following contributing factors were reported:
- Overload failure,
- Pilot-in-command previously held commercial mel and agricultural operator certificates.
Final Report:

Crash of a Beechcraft 65 Queen Air near Preston: 1 killed

Date & Time: Jun 13, 1979 at 2000 LT
Type of aircraft:
Operator:
Registration:
N111WP
Flight Phase:
Flight Type:
Survivors:
No
MSN:
LC-132
YOM:
1962
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
333
Circumstances:
While in normal cruise, one of the engine failed due to low compression. The pilot reduced his altitude and attempted an emergency landing when the airplane crashed near Preston. The pilot, sole on board, was killed. A load of marijuana and drugs was found on board the aircraft that was stolen.
Probable cause:
Engine failure for undetermined reasons. The following contributing factors were reported:
- Inadequate maintenance and inspection on part of the maintenance personnel,
- Low compression,
- Stolen aircraft,
- Illegal flight,
- Forced landing off airport on land,
- Complete engine failure.
Final Report:

Crash of a Lockheed 18 LodeStar in Lincolnton

Date & Time: Apr 12, 1979 at 0645 LT
Type of aircraft:
Registration:
N250W
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
2025
YOM:
1940
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll, the crew decided to abandon the takeoff procedure. Unable to stop within the remaining distance, the twin engine airplane overran, struck trees and crashed in flames. Both occupants were seriously injured and the aircraft was destroyed by fire. A load of 2,000 lbs of marijuana was found on board.
Probable cause:
Collision with trees after an aborted takeoff because the crew delayed action in aborting takeoff.
Final Report:

Crash of a Percival P.66 Pembroke in Sylvester

Date & Time: Aug 3, 1978
Type of aircraft:
Operator:
Registration:
N51951
Flight Type:
Survivors:
Yes
MSN:
20
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Sole on board, the pilot was completing a drug smuggling flight from Colombia, originally to Valdosta, Georgia. The aircraft was carrying a load of 2,000 lbs of marijuana and supposed to land at Valdosta Airport. For unknown reasons, the runway lights could not be activated so the pilot diverted to Sylvester Airport where the visibility was about half a mile in fog. After landing, the twin engine airplane went out of control, veered off runway and came to rest. The pilot deliberately burnt the aircraft after accident.
Final Report:

Crash of a Douglas DC-3C near Newton

Date & Time: Jun 13, 1977 at 0030 LT
Type of aircraft:
Registration:
N38AP
Flight Type:
Survivors:
Yes
MSN:
10217
YOM:
1943
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot attempted to land by night on an unsuitable terrain located near Newton that was lighted by flashlights. Upon landing, the gear collapsed and the airplane crashed. The passenger was slightly injured while the pilot was seriously wounded. The aircraft was written off. This was probably a drug smuggling flight.
Probable cause:
Gear collapsed on landing after the pilot selected an unsuitable terrain. The following contributing factors were reported:
- Misjudged distance and speed,
- Not aligned with the intended landing area,
- Intentional ground loop,
- Overload failure,
- Landing area lighted by flashlights.
Final Report:

Crash of a Douglas DC-9-31 in New Hope: 72 killed

Date & Time: Apr 4, 1977 at 1619 LT
Type of aircraft:
Operator:
Registration:
N1335U
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Muscle Shoals - Huntsville - Atlanta
MSN:
47393
YOM:
1970
Flight number:
SO242
Crew on board:
4
Crew fatalities:
Pax on board:
81
Pax fatalities:
Other fatalities:
Total fatalities:
72
Captain / Total flying hours:
19380
Captain / Total hours on type:
3205.00
Copilot / Total flying hours:
3878
Copilot / Total hours on type:
235
Aircraft flight hours:
15405
Circumstances:
Southern Airways Flight 242, a DC-9-31, operated as a scheduled passenger flight from Muscle Shoals, Alabama, to Atlanta, Georgia, with an intermediate stop at Huntsville, Alabama. Flight 242 departed Muscle Shoals at 15:21 and landed at Huntsville about 15:44. About 15:54, Flight 242 departed Huntsville on an instrument flight rules (IFR) flight plan for the Hartsfield-Atlanta International Airport; there were 81 passengers and 4 crew members aboard. The flight's route was direct to the Rome VOR and then a Rome runway 26 profile descent to Atlanta. Its estimated time en route was 25 min and its requested en route altitude was 17,000 ft. At 15:56, the controller told Flight 242 that his radarscope was showing heavy precipitation and that the echos were about 5 nmi ahead of the flight. At 15:57:36, the controller said, "...you're in what appears to be about the heaviest part of it now, what are your flight conditions." Flight 242 replied, "...we're getting a little light turbulence and...I'd say moderate rain." At 15:57:47, the controller acknowledged Flight 242's report and told the flight to contact Memphis Center. The Memphis Center controller advised the flight that a SIGMET was current for the area. He then told Flight 242 to contact Atlanta Center. At 16:03:20, Flight 242 switched to another sector of Atlanta Center, established communications on the new frequency and reported being level at FL170. As the aircraft entered an area of rain, the flight crew began discussing the weather depicted on their radar. Based on information from the airborne radar, the captain initially decided that the storms just west of the Rome VOR were too severe to penetrate. Shortly after his initial assessment of the storm system, the captain decided to penetrate the storm area near the Rome VOR. At 16:06:41 Atlanta Center cleared Flight 242 to descend to and maintain 14,000 ft. Shortly afterwards the aircraft entered an area of heavy hail or rain, which continued for at least one minute. The ingestion of intense rain and hail into the engines caused the rotational speed of both engines to decrease below the engine-driven electrical generator operating speeds, and resulted in normal electrical power interruption for 36 seconds. The flight crew likely advanced one or both thrust levers, restoring its generator to operation and provide normal electrical power. After establishing contact with Atlanta Center again, the flight was told to maintain 15,000 ft. At 16:09:15, Flight 242 reported to Atlanta Center, "Okay...we just got our windshield busted and... we'll try to get it back up to 15, we're 14." After reported that the left engine had flamed out, the flight was cleared to descend to 13,000 ft. Meanwhile both engines' high-pressure compressors began to stall severely due to ingestion of massive quantities of water. The severe compressor stalls produced an overpressure surge which deflected the compressor blades forward in the sixth stage of the low-pressure compressors; these blades clashed against the fifth-stage stator vanes and broke pieces from the blades and vanes. Pieces of blades and stator vanes were then ingested into the high-pressure compressors and damaged them severely. Continued high thrust settings following the severe damage to the high-pressure compressors probably caused severe overheating in the turbine sections of both engines, and the engines ceased to function. Shortly before normal electrical power was again, the flight crew radioed that both engines had failed. Atlanta Center told the crew to contact approach control for vectors to Dobbins Air Force Base. Power was then lost for 2 min 4 sec until the APU-driven generator restored electrical power. After establishing contact with Atlanta Approach Control the flight was told they were 20 miles from Dobbins. As the flight was descending, the captain began to doubt their ability to reach Dobbins. Cartersville was closer at 15 miles, so the controller gave vectors for Cartersville. Unable to make it to Cartersville, the crew began looking for a clear field or highway for an emergency landing. At 16:18:02, Flight 242's last transmission to Approach Control was recorded: "... we're putting it on the highway, we're down to nothing." The aircraft's outboard left wing section first contacted two trees near State Spur Highway 92 south-southwest of the community of New Hope. About 0.8 miles farther north-northeast, the left wing again contacted a tree alongside the highway within the community of New Hope. The left and right wings continued to strike trees and utility poles on both sides of the highway, and 570 ft after striking the first tree in New Hope, the aircraft's left main gear contacted the highway to the left of the centerline. Almost simultaneously, the outer structure of the left wing struck an embankment, and the aircraft veered to the left and off the highway. The aircraft traveled another 1,260 ft before it came to rest. As it traveled, the aircraft struck road signs, utility poles, fences, trees, shrubs, gasoline pumps at a gas station-store, five automobiles, and a truck. Of the 85 persons aboard Flight 242, 62 were killed, 21 were seriously injured, and 1 was slightly injured. Additionally, eight persons on the ground were killed. Within a month of the accident, one of the surviving passengers and one person on the ground both died of their injuries.
Probable cause:
Total and unique loss of thrust from both engines while the aircraft was penetrating an area of severe thunderstorms. The loss of thrust was caused by the ingestion of massive amounts of water and hail which, in combination with thrust lever movement, induced severe stalling in and major damage to the engine compressors. Major contributing factors include the failure of the company's dispatching system to provide the flight crew with up-to-date severe weather information pertaining to the aircraft's intended route of flight, the captain's reliance on airborne weather radar for penetration of thunderstorm areas, and limitations in the FAA's ATC system which precluded the timely dissemination of real-time hazardous weather information to the flight crew.
Final Report:

Crash of a Mitsubishi MU-2-30 Marquise in Augusta

Date & Time: Apr 1, 1977 at 1620 LT
Type of aircraft:
Registration:
N100SW
Flight Type:
Survivors:
Yes
Schedule:
Atlanta - Augusta
MSN:
539
YOM:
1971
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Circumstances:
The crew was completing a ferry flight from Atlanta to Augusta. On approach to Augusta Airport, both engines flamed out almost simultaneously. The crew elected to make an emergency landing when the airplane struck trees and crashed in rough terrain. The aircraft was destroyed and both occupants were seriously injured.
Probable cause:
Double engine failure on final approach due to fuel exhaustion. The following contributing factors were reported:
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Inattentive to fuel supply,
- Fuel exhaustion,
- Rough terrain.
Final Report: