Date & Time: Dec 9, 2004 at 1831 LT
Operator:
RNH Air 1
Registration:
N6PE
Survivors:
Yes
Schedule:
La Crosse – Tulsa
MSN:
BB-856
YOM:
1981
Crew on board:
1
Crew fatalities:
0
Pax on board:
0
Pax fatalities:
0
Other fatalities:
0
Total fatalities:
0
Captain / Total flying hours:
2089
Captain / Total hours on type:
469
Aircraft flight hours:
3084
Circumstances:
The 2,100-hour instrument-rated private pilot stated that prior to departure for a 507 nautical mile cross-country flight, the fuel gauges indicated approximately 800 pounds of fuel on each side for a total of 1600 pounds; however, he did not visually check the amount of fuel that the tanks contained. During his approach to the destination airport, the right engine started to "sputter" before it finally quit. The pilot then "looked over at the fuel gauges and both tanks were showing empty." The left engine quit just a few moments later. The auto ignition installed in the airplane attempted to restart the engines. The engines restarted momentarily and then shut-off once more. The pilot declared an emergency and executed a forced landing onto a street below. After a hard landing onto the street, the right wing hit a telephone pole, and the left wing then hit several tree limbs before the airplane impacted a hill and came to a stop. The Federal Aviation Administration (FAA) inspector, who responded to the accident site, found the fuel transfer switch in the "right-crossfeed" position. The fuel system was examined and no leaks or anomalies were found. Approximately three-quarters of a gallon of unusable fuel was found in the right engine nacelle. Approximately four gallons (28 pounds) of usable fuel was found in the left engine nacelle.
Probable cause:
The loss of engine power due to fuel exhaustion as a result of the pilot's inadequate preflight and in-flight planning / preparation.
Final Report:
N6PE.pdf102.87 KB