Crash of a Rockwell Grand Commander 680FL near Fort Collins: 1 killed

Date & Time: Sep 12, 1985 at 0020 LT
Registration:
N45724
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Fort Collins - Salt Lake City
MSN:
680-1291-2
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3554
Captain / Total hours on type:
43.00
Aircraft flight hours:
9535
Circumstances:
The pilot was operating his aircraft under the rules of 14 cfr 135, i.e., a scheduled domestic cargo flight. He made a normal departure and climb en route to Salt Lake City, UT. Normal communications and radar flight following was established with Denver ARTCC. Approximately 8 miles west of fort collins, the aircraft suddenly disappeared off of radar and voice contact with the pilot was lost.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: climb - to cruise
Findings
1. Light condition - dark night
2. (c) reason for occurrence undetermined
3. Weather condition - turbulence
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
4. Reason for occurrence undetermined
Final Report:

Crash of a Cessna 404 Titan II near Hayesville: 1 killed

Date & Time: Sep 11, 1985 at 0105 LT
Type of aircraft:
Operator:
Registration:
N128SP
Flight Phase:
Flight Type:
Survivors:
No
Site:
MSN:
404-0429
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Fisherman heard an aircraft overhead but did not see any sign of it in the night sky. Shortly thereafter they saw a flash and fire on the side of a mountain, then they heard the explosion. The sheriff was called and an investigation revealed a crashed aircraft. There were no signs of occupants in or near the aircraft. The next morning the body of a heavily armed man who had on a parachute and a deployed reserve parachute was found several miles away in a residential area. A key to the crashed aircraft was found on the body.
Probable cause:
Occurrence #1: miscellaneous/other
Phase of operation: cruise - normal
Findings
1. (c) aircraft handling
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
2. Terrain condition - mountainous/hilly
3. (c) aircraft unattended/engine(s) running - intentional - pilot in command
----------
Occurrence #3: fire/explosion
Phase of operation: other
Final Report:

Crash of a Douglas TC-47J near Naples

Date & Time: Sep 10, 1985
Operator:
Registration:
N846MB
Flight Phase:
Survivors:
Yes
Schedule:
Naples - Naples
MSN:
33305/16557
YOM:
1945
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While engaged in a mosquito control flight, the right engine failed. The crew attempted an emergency landing when the aircraft crash landed east of Naples. Both crew members escaped uninjured while the aircraft was damaged beyond repair. Registration to be confirmed.
Probable cause:
Engine failure in flight for unknown reasons.

Crash of a Douglas DC-9-14 in Milwaukee: 31 killed

Date & Time: Sep 6, 1985 at 1521 LT
Type of aircraft:
Operator:
Registration:
N100ME
Flight Phase:
Survivors:
No
Schedule:
Milwaukee - Atlanta
MSN:
47309
YOM:
1968
Flight number:
YX105
Crew on board:
4
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
31
Captain / Total flying hours:
5100
Captain / Total hours on type:
1100.00
Copilot / Total flying hours:
5197
Copilot / Total hours on type:
1640
Aircraft flight hours:
31892
Aircraft flight cycles:
48903
Circumstances:
Midwest Express Airlines Flight 206, DC-9 N100ME arrived at Milwaukee (MKE) at 13:15 on September 6, 1985. It departed Milwaukee at 13:36 and arrived in Madison at 13:55 after an uneventful flight. At Madison, N100ME was designated as flight 105 to Atlanta (ATL), with an intermediate stop in Milwaukee. Flight 105 departed Madison at 14:25 and arrived at Milwaukee, on time and without incident, at 14:41. About 14:49, the first officer of flight 105 contacted Milwaukee Tower to request an instrument flight rule (IFR) clearance to Atlanta. The clearance was received. The Atlanta forecast included a 1,000-foot ceiling, visibility 2 miles, thunderstorms and rain showers. At 15:12, the Before Engine Start Checklist was read and accomplished in accordance with Midwest Express operating procedures. Engine start was commenced at 15:14 and the After Start Checklist was accomplished. The first officer requested clearance to taxi to runway 19R for departure. About 15:17:50, the Taxi Checklist was completed, and the engine pressure ratio (EPR) and airspeed reference bugs were set to 1.91 and 133 knots, respectively. Both indications were correct for the departure conditions applicable to flight 105. At the conclusion of the Taxi Checklist, the captain advised the first officer "Standard briefing ..." At 15:19:15, the first officer reported to the tower local controller, "Milwaukee, Midex 105, ready on 19R." Flight 105 was cleared to "position and hold" on runway 19R. The captain called for the Before Takeoff Checklist, which was completed in accordance with the COM. Flight 105 was cleared for takeoff at 15:20:28; the first officer acknowledged the clearance. The captain operated the flight controls, and the first officer handled radio communications and other copilot responsibilities during the takeoff. The Midwest Express DC-9 Flight Operations Manual required the use of standard noise abatement takeoff procedures during all line operations, unless precluded by safety considerations or special noise abatement procedures. At the time flight 105 departed, noise abatement procedures were in effect. Midwest Express also utilized "reduced thrust" takeoff procedures (at the captain's discretion) to extend engine life. The flightcrew was complying with the reduced thrust and standard noise abatement takeoff procedures. The takeoff roll and liftoff were normal, with liftoff occurring near the intersection of the midfield taxiway and runway 19R, about 4,200 feet from the start of the takeoff roll. Rotation to the takeoff attitude occurred at 140 knots. The DC-9 accelerated to 168 knots with a rate of climb of about 3,000 feet/minute, indicating a normal two-engine initial takeoff flightpath. At 15:21:26 N100ME was about 7,600 feet down the runway, reaching a height of 450 feet above the ground. At that moment there was a loud noise and a noticeable decrease in engine sound. The captain then remarked "What the # was that?" The first officer did not respond. At 15:21:29, the local controller transmitted, "Midex 105, turn left heading 175." At the time of his transmission he observed smoke and flame emanating from the right airplane engine. The captain asked the first officer, "What do we got here, Bill?" The first officer did not respond to the captain but advised the local controller, "Midex 105, roger, we've got an emergency here." Two seconds later, the captain said, "Here"; again there was no response. Neither pilot made the call outs for "Max Power" or "Ignition Override-Check Fuel System," which were part of the Midwest Express "Engine Failure after V1" emergency procedure. Meanwhile the airplane began to deviate substantially to the right and the heading changed from 194 degrees to 260 degrees in eight seconds. The vertical acceleration dropped sharply to about 0.3 G and increased to a value of 1.8 G. At that point the airplane stalled. This accelerated stall occurred at a KIAS of about 156 kts.
Probable cause:
The flight crew's improper use of flight controls in response to the catastrophic failure of the right engine during a critical phase of flight, which led to an accelerated stall and loss of control of the airplane. Contributing to the loss of control was a lack of crew coordination in response to the emergency. The right engine failed from the rupture of the 9th to 10th stage removable sleeve spacer in the high pressure compressor because of the spacer's vulnerability to cracks.
Final Report:

Crash of a Cessna T303 Crusader in Simi Valley

Date & Time: Aug 30, 1985 at 1736 LT
Type of aircraft:
Registration:
N6490V
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Santa Monica - Santa Monica
MSN:
303-00312
YOM:
1984
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3365
Captain / Total hours on type:
127.00
Aircraft flight hours:
2
Circumstances:
The aircraft collided with trees during a forced landing following a loss of power. The student pilot stated the flight was normal until a 'violent right yaw' developed when the throttles were advanced to recover from a practice stall. As the cfi took over the controls and attempted recovery a 'substantial loss of power' occurred on both engines. A forced landing was made in a field during which the left wing contacted trees and the aircraft was engulfed in flames. Post accident examination of the left engine failed to disclose any discrepancies. Discrepancies were noted on the right engine.
1) The fuel controller fuel line 'tee' fitting was cracked around 50% of its circumference. (ductile overload).
2) The turbocharger gasket on the inlet side of the turbine showed leakage around 70% of the gasket are. The aircraft had a history of symptoms of fuel vaporization which subsided with use of the aux fuel pump as the engine manufacturer suggests. It is unknown if the aux pump was used during this accident.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: maneuvering
Findings
1. (f) fuel system,line - leak
2. (c) maintenance, installation - improper - manufacturer
3. (f) exhaust system, turbocharger - leak
4. (f) fuel system, line fitting - cracked
5. Fluid, fuel - starvation
6. (f) weather condition - temperature extremes
----------
Occurrence #2: loss of engine power (total) - non mechanical
Phase of operation: maneuvering
Findings
7. (f) fluid, fuel - starvation
8. (f) weather condition - temperature extremes
----------
Occurrence #3: in flight collision with object
Phase of operation: descent - emergency
Findings
9. (f) object - tree(s)
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
Final Report:

Crash of a Beechcraft C99 Airliner in Conover: 3 killed

Date & Time: Aug 28, 1985 at 0145 LT
Type of aircraft:
Operator:
Registration:
N992SB
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Hickory - Charlotte
MSN:
U-170
YOM:
1981
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5309
Captain / Total hours on type:
950.00
Aircraft flight hours:
7651
Circumstances:
Aircraft was on training flight for initial copilot qualification for commuter air carrier. Instructor and two trainees were on board. The aircraft departed Charlotte at about 2314 edt for the Hickory area for training. At about 0015 edt, it was reported that the crew visited the Hickory FSS. After departing Hickory, the aircraft climbed to 5,500 feet and remained generally between Charlotte. At about 0145 edt, radar data showed the aircraft to be in a steep descent and gaining speed. The aircraft collided with tree limbs, a utility pole and the ground in about 35° angle of descent in a residential area of Conover, NC. Investigation revealed a nose up trim, which was approximately 75% of the available up-trim (3.38° upnose). This is an abnormal setting; so the entire trim unit was retained and sent to the Talley Corp for detailed exam. The ram end fittings were sent to ga tech research for surface fracture analysis. The exam showed ductile overstress and no indication of pre-cracked condition. Pitch trim emergencies are a part of sunbirds c-99 training program (fit 1 & 2). All three occupants were killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise
Findings
1. (c) emergency procedure - selected - pilot in command (cfi)
2. (c) remedial action - not performed - dual student
3. (c) lack of familiarity with aircraft - dual student
4. (c) remedial action - delayed - pilot in command (cfi)
5. (c) fatigue (flight and ground schedule) - pilot in command (cfi)
6. (c) supervision - not maintained - pilot in command (cfi)
7. (f) complacency - pilot in command (cfi)
8. (c) fatigue (flight and ground schedule) - pilot in command (cfi)
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Boeing KC-135A-BN Stratotanker at Beale AFB: 7 killed

Date & Time: Aug 27, 1985
Type of aircraft:
Operator:
Registration:
59-1443
Flight Type:
Survivors:
No
Schedule:
Beale - Beale
MSN:
17931
YOM:
1960
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Aircraft flight hours:
9936
Circumstances:
The crew was dispatched at Beale AFB to follow a training program. Following several touch-and-go maneuvers, the crew started a new approach when the aircraft became unstable on final. The instructor allowed the pilot-in-command to continue the approach when the engine n°1 struck the runway surface, caught fire and exploded. Out of control, the airplane banked left and crashed, bursting into flames. All seven crew members were killed.

Crash of a Beechcraft 99 Airliner in Auburn: 8 killed

Date & Time: Aug 25, 1985 at 2205 LT
Type of aircraft:
Operator:
Registration:
N300WP
Survivors:
No
Schedule:
Boston - Auburn
MSN:
U-22
YOM:
1968
Flight number:
QO1808
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
5153
Captain / Total hours on type:
4467.00
Copilot / Total flying hours:
1453
Copilot / Total hours on type:
153
Aircraft flight hours:
30335
Circumstances:
Flight 1808 took off from Boston runway 04L at 21:30 for a flight to Auburn. Clearance was received of 7000 feet and to contact Portland Approach Control. Portland Approach cleared Flight 1808 at 21:58 for a runway 04 ILS approach. Three minutes later the controller noticed that Flight 1808 was east of course and asked if the it was receiving the Lewiston localizer. The captain replied that they hadn't and were given instructions to turn left heading 340. A left turn to 354° started and the aircraft passed Lewie Outer Marker (LOM) at 165 knots, 2,600 feet (30 knots too fast and 600 feet too high). At 22:02 the aircraft exited the left side of the localizer, still at a 354° heading. The crew then tried to capture the glide slope and enter the localizer again until it entered the left side of the localizer (22:04:08) and descended through the bottom boundary of the glide slope. At ca 22:04:16 the aircraft struck trees 4,007 feet short of the runway and 440 feet right of the extended centreline, continued 737 feet and struck level ground in nearly an inverted attitude. One of the passengers killed in the crash was American schoolgirl, peace activist and child actress Samantha Smith. She was returning to Auburn with her father after taking part to a TV movie in Boston.
Probable cause:
The captain's continuation of an unstabilized approach which resulted in a descent below glide slope. Contributing to the unstabilized approach was the radar controller's issuance and the captain's acceptance of a non-standard air traffic control radar vector resulting in an excessive intercept with the localizer.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in San Angelo

Date & Time: Aug 24, 1985 at 1700 LT
Registration:
N8045J
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Angelo - San Angelo
MSN:
61-0528-222
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1386
Captain / Total hours on type:
35.00
Aircraft flight hours:
897
Circumstances:
The pilot had recently purchased the aircraft and received 25 hours dual instruction to comply with his insurance requirements. Shortly thereafter he went out solo to practice steep turns. He climbed to 12,500 feet and leveled off. He then rolled into a 60° left bank at 200 knots airspeed by applying left aileron and back pressure. He then applied moderate left rudder. At this time the nose came up, the right wing came over the top, the nose tucked down and the aircraft entered a steep nose down spin. In his attempt to stop the spin the pilot shut down both engines. He got the spin stopped after 15 to 20 turns. He started pulling the nose up and the stall buffet was felt. Alt was 500 feet agl at this time and he was unable to restart the engines. He then made a gear up landing in a pasture which resulted in destruction of the aircraft. The pilot was uninjured.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: maneuvering
Findings
1. (c) stall/spin - inadvertent - pilot in command
2. (f) in-flight planning/decision - poor - pilot in command
3. (c) lack of total experience in type of aircraft - pilot in command
----------
Occurrence #2: loss of engine power
Phase of operation: descent - uncontrolled
Findings
4. (c) powerplant controls - improper use of - pilot in command
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
Findings
5. (f) terrain condition - rough/uneven
6. (c) wheels up landing - intentional - pilot in command
Final Report:

Crash of a Piper PA-31T Cheyenne II near Flat Rock: 5 killed

Date & Time: Aug 23, 1985 at 2155 LT
Type of aircraft:
Registration:
N600CM
Flight Phase:
Survivors:
No
Site:
Schedule:
Louisville - Greer
MSN:
31-7720024
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1700
Aircraft flight hours:
4077
Circumstances:
Aircraft hit northwest side of ridge in level attitude, cruise speed, heading southeast. Conditions were dark night and the cloud ceiling was about 40 feet above the ridge. Pilot received weather brief before take off and en route which reported a ceiling of 10,000 feet at destination. Aircraft was flown at 17,500 feet en route. Pilot-in-command radioed GSP approach control, said he was VFR for landing, passing 6,000 feet. Two way communication not established but discrete tx code assigned. Controller saw tx code change northwest of crash site then radar target disappeared at accident site. All five occupants were killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: cruise
Findings
1. (c) ifr procedure - disregarded - pilot in command
2. (c) descent - premature - pilot in command
Final Report: