Crash of an Embraer EMB-110P1 Bandeirante in Alpena: 3 killed

Date & Time: Mar 13, 1986 at 2200 LT
Operator:
Registration:
N1356P
Survivors:
Yes
Schedule:
Detroit - Alpena - Saulte Sainte Marie
MSN:
110-370
YOM:
1981
Flight number:
MQ1746
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3384
Captain / Total hours on type:
574.00
Copilot / Total flying hours:
6271
Copilot / Total hours on type:
21
Aircraft flight hours:
9698
Aircraft flight cycles:
16767
Circumstances:
About 2050 on March 13, 1986, Simmons Airlines flight 1746, an Embraer Bandeirante, EMB-110P1, operating as a regularly scheduled flight, departed the Detroit Metropolitan Airport en route to Sault Ste Marie, Michigan, with a stop in Alpena, Michigan. The en route portion of the flight to Alpena was uneventful. However, due to the prevailing instrument meteorological conditions, the crew was unable to complete the instrument landing system (ILS) approach and land and they declared a missed approach at 2142. At 2153, the flight was cleared for a second ILS approach to Alpena. At 2156, the crew acknowledged that radar services were being terminated. This was the last transmission from the airplane. About 2215, a motorist reported that the airplane had
crashed. The airplane was found in a wooded area about 300 feet to the left of the extended centerline, and 1 1/2 miles short of the threshold of runway 01 at Alpena. The airplane was destroyed and two of the seven passengers and one of the two crewmembers onboard were killed.
Probable cause:
The National Transportation Safety Board determines that the probable cause of this accident was the flightcrew’s continued descent of the airplane below the glideslope and through the published decision height without obtaining visual reference of the runway for undetermined reasons. Contributing to the accident was the inefficient system used to disseminate weather-related information to the crew.
Final Report:

Crash of a Cessna 401 in Silver City

Date & Time: Mar 13, 1986 at 2007 LT
Type of aircraft:
Registration:
N9867F
Flight Type:
Survivors:
Yes
Schedule:
Scottsdale - Silver City
MSN:
401-0301
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16400
Captain / Total hours on type:
1800.00
Aircraft flight hours:
5990
Circumstances:
The two commercial rated pilots were returning from a part 135 flight at night. The fuel tanks were inadvertently not switched from mains to auxiliary. Fuel starvation occurred when aircraft was at low altitude. Insufficient altitude remained to restart the engines. Aircraft impacted ground. A post accident fire erupted destroying the aircraft. Both pilots were seriously injured.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: maneuvering
Findings
1. (c) fluid,fuel - starvation
2. (c) checklist - not followed - copilot/second pilot
3. (c) pilot in command
4. (c) fuel tank selector position - improper - copilot/second pilot
5. (c) supervision - inadequate - pilot in command
----------
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
Findings
6. (f) terrain condition - none suitable
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise in Eola: 5 killed

Date & Time: Mar 5, 1986 at 1706 LT
Type of aircraft:
Operator:
Registration:
N513DC
Flight Phase:
Survivors:
No
Schedule:
Chicago – DuPage
MSN:
321
YOM:
1975
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
4590
Captain / Total hours on type:
180.00
Circumstances:
Evidence shows copilot called, 'mayday, uncontrolled spin' after aIRCRAFT radar track showed decelERATION from 180 to 120 kNOts over 2 minUTES period while maintaining constant 4,000 feet cruise altitude. Constant altitude consistent with autopilot/autotrim use, particularly in view of reported turbulence/icing. Elevator trim found at approx 13° nose up. No evidence found of preimpact failure or malfunction in aircraft powerplants, structure or systems. Evidence suggests scenario of crew inattention after power reduction with autopilot altitude setting. On power application, aircraft pitched up from slow speed into uncontrolled flight. Duty day at time of mishap approaching 11 hours. All five occupants were killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise
Findings
1. (c) aircraft handling - not maintained - pilot in command
2. (f) fatigue (flight and ground schedule) - pilot in command
3. (f) throttle/power control - improper use of - pilot in command
4. (f) trim setting - improper - pilot in command
5. (f) weather condition - icing conditions
6. (f) weather condition - turbulence
7. Stall/spin
Final Report:

Crash of a Learjet 24D off San Clemente Island: 2 killed

Date & Time: Mar 5, 1986
Type of aircraft:
Operator:
Registration:
N97DM
Flight Phase:
Flight Type:
Survivors:
No
MSN:
24-253
YOM:
1972
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was engaged in a military exercise consisting of an aerial attack of a US Navy vessel. In unknown circumstances, the aircraft collided with a second Flight International Learjet 35 registered N39DM. Both aircraft crashed in the sea about 27 miles southeast of San Clemente Island and all four crew members were killed.
Probable cause:
In-flight collision for unknown reasons.

Crash of a Learjet 35 off San Clemente Island: 2 killed

Date & Time: Mar 5, 1986
Type of aircraft:
Operator:
Registration:
N39DM
Flight Phase:
Flight Type:
Survivors:
No
MSN:
35-040
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was engaged in a military exercise consisting of an aerial attack of a US Navy vessel. In unknown circumstances, the aircraft collided with a second Flight International Learjet 24D registered N97DM. Both aircraft crashed in the sea about 27 miles southeast of San Clemente Island and all four crew members were killed.
Probable cause:
In-flight collision for unknown reasons.

Crash of a Dassault Falcon 10 in Coatesville

Date & Time: Feb 27, 1986 at 2230 LT
Type of aircraft:
Operator:
Registration:
N821LG
Survivors:
Yes
Schedule:
New York-JFK – Lexington
MSN:
170
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8260
Captain / Total hours on type:
963.00
Aircraft flight hours:
1447
Circumstances:
As the aircraft was climbing thru 19,000 feet at night, the #2 generator (gen) light came on. The flight crew noted there was no output from the #2 gen and it would not reset. They then checked the #1 gen voltage and noted it was 14 to 15 volts. The crew reduced the electrical load; however, about 5 minutes later, the batteries became discharged and there was a total loss of electrical power. Using a flashlight, the crew diverted to the Chester County Airport which had a 4,600 feet runway. The gear was extended with the emergency system. The elevator trim was inoperative, so both pilots applied back pressure on the yoke to overcome the nose down tendency. After landing about 1/4 of the way down the runway, the crew tried to use the thrust reversers, but the reversers were inoperative. Subsequently, the aircraft continued off the side and beyond the end of the runway, hit a wooden beam and a snowbank, then came to rest in a ditch. An investigation revealed a shaft failure of the #2 gen (starter/gen) and worn brushes in the #1 gen. With total electrical failure, the following were also inoperative: wing flaps, anti-skid, capt's airspeed indicator and altimeter, nose wheel steering, cockpit lighting.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: cruise
Findings
1. (f) maintenance - inadequate - other maintenance personnel
2. (c) electrical system, generator - worn
3. (c) electrical system, generator - failure,total
4. Electrical system, battery - exhaustion
5. Electrical system - inoperative
6. Comm/nav equipment - inoperative
7. Flt control syst, stabilator trim - inoperative
8. Flight control, flap - inoperative
9. Landing gear, steering system - inoperative
10. Landing gear, anti-skid brake system - inoperative
11. Thrust reverser - inoperative
----------
Occurrence #2: loss of control - on ground/water
Phase of operation: landing - roll
Findings
12. (f) light condition - dark night
13. Performed
14. Precautionary landing - performed
15. (f) directional control - not maintained - pilot in command
16. Ground loop/swerve - uncontrolled
----------
Occurrence #3: overrun
Phase of operation: landing - roll
Findings
17. (f) powerplant controls - improper use of - pilot in command
----------
Occurrence #4: on ground/water collision with object
Phase of operation: landing - roll
----------
Occurrence #5: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Final Report:

Crash of a Beechcraft G18S in Janesville

Date & Time: Feb 26, 1986 at 0516 LT
Type of aircraft:
Operator:
Registration:
N723T
Flight Type:
Survivors:
Yes
Schedule:
Detroit - Janesville
MSN:
BA-579
YOM:
1961
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Captain / Total hours on type:
5700.00
Aircraft flight hours:
11676
Circumstances:
The aircraft impacted the ground about 1,000 feet to the left of the runway. The pilot stated that he did not have visual contact with the ground and remembers attempting to make a missed approach. Conditions were IMC. The pilot was seriously injured and the aircraft was destroyed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: missed approach (ifr)
Findings
1. (c) decision height - below - pilot in command
2. (c) missed approach - delayed - pilot in command
3. Motivation - pilot in command
4. (f) weather condition - obscuration
5. (f) weather condition - low ceiling
6. Light condition - dawn
Final Report:

Crash of a Beechcraft G18S in Copperhill: 1 killed

Date & Time: Feb 22, 1986 at 0627 LT
Type of aircraft:
Operator:
Registration:
N74FA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Kenosha - Milwaukee - Atlanta
MSN:
BA-504
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7500
Captain / Total hours on type:
2500.00
Aircraft flight hours:
14640
Circumstances:
The pilot was alerted at 0100 for 0200 flight from Kenosha to Milwaukee, WI to pick up cargo for a flight to Atlanta, GA. At 0310, the aircraft departed Milwaukee in VFR. En route, the pilot obtained weather and an IFR clearance. Some of his radio transmissions were not standard. At 0433, he complied with ATC request for frequency change, but his radio transmissions were not clear. Approximately 5 minutes later, ATC asked the pilot to change frequency again, but 5 calls were made before he replied. His last transmission was at 0445:48; he didn't respond to further ATC calls. The aircraft continued cruising at 11,000 feet until 0621, then it descended without clearance. Radar contact was lost at 0627 cst (0727 est). Shortly thereafter, it impacted trees on a mountain, then crashed to the ground and burned. A witness believed the engines were throttled back before impact. Also, the witness reported low clouds and fog, but said the mountain was visible and was not obscured. The pilot had a 1,58‰ alcohol level in blood, no sleep for 21.5 hours, history of alcohol abuse, 7 prior dwi convictions (and ndr rec). Also, he falsified FAA medical applications. FAA was advised in 1984, but took no action.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise - normal
Findings
1. (c) preflight planning/preparation - inadequate - pilot in command
2. (c) impairment (alcohol) - pilot in command
3. (f) fatigue - pilot in command
4. (f) fatigue (flight schedule) - company/operator management
5. (f) insuff standards/requirements, operation/operator - company/operator mgmt
6. (f) inadequate surveillance of operation - faa (organization)
7. (c) judgment - poor - pilot in command
8. (f) company-induced pressure - company/operator management
9. (f) procedures/directives - not followed - pilot in command
10. (c) descent - uncontrolled - pilot in command
11. (f) fatigue (lack of sleep) - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
12. Terrain condition - mountainous/hilly
13. Object - tree(s)
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Douglas DC-9-31 in Erie

Date & Time: Feb 21, 1986 at 0859 LT
Type of aircraft:
Operator:
Registration:
N961VJ
Survivors:
Yes
Schedule:
Toronto - Erie
MSN:
47506
YOM:
1970
Flight number:
US499
Crew on board:
5
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8900
Captain / Total hours on type:
5900.00
Aircraft flight hours:
42104
Circumstances:
During arrival, the crew of USAir flight 499 landed on runway 24, which was covered with snow. Reportedly, while landing, the aircraft touched down approximately 1,800 to 2,000 feet beyond the displaced threshold. Altho armed, the spoilers did not autodeploy, so the captain operated them manually. He lowered the aircraft's nose, actuated reverse thrust and applied brakes. The brakes were not effective. Subsequently, the aircraft continued off the end of the runway, ran over a runway end id light, struck a fence and came to rest straddling a road. The crew had planned on making an ILS approach to runway 06, but the RVR was only 2,800 feet and a minimum RVR of 4 000 feet was requested for that runway. The crew elected to land on runway 24, since 1/2 mile visibility was sufficient for that runway. However, the approach was made with a qtrg tailwind and approximately 10 knots above Vref. Tailwind landings were not authorized on runway 24 in wet/slippery conditions. The runway braking action was reported as fair-to-poor. The pilot's handbook cautioned the crew to monitor the spoilers when landing on slippery runways, since the spoilers auto-deploy only with wheel spin-up or when the nose wheel is on the ground. A passenger was slightly injured while 22 other occupants were uninjured.
Probable cause:
Occurrence #1: overrun
Phase of operation: landing - roll
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - snow
3. (f) weather condition - fog
4. (f) weather condition - tailwind
5. (c) planning/decision - improper - pilot in command
6. (f) airspeed(vref) - exceeded - pilot in command
7. (f) airport facilities, runway/landing area condition - displaced threshold
8. (f) proper touchdown point - not attained - pilot in command
9. (f) airport facilities, runway/landing area condition - snow covered
10. (c) go-around - not performed - pilot in command
----------
Occurrence #2: on ground/water collision with object
Phase of operation: landing - roll
Findings
11. (f) object - runway light
12. (f) object - fence
----------
Occurrence #3: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
13. (f) terrain condition - rough/uneven
Final Report:

Crash of a Piper PA-31-310 Navajo in Moore Haven: 2 killed

Date & Time: Feb 17, 1986
Type of aircraft:
Operator:
Registration:
N7EA
Flight Phase:
Flight Type:
Survivors:
No
MSN:
31-117
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
On February 17, 1986 the wreckage of N7EA along with the skeletal remains of two persons were found. The aircraft crashed into trees causing the separation of the outboard six feet of left wing and then continued crashing through more trees before colliding with the ground. The aircraft caught fire during the impact sequence and was completely destroyed by post crash fire. Fuel fittings and pumps used in aircraft fuel systems were found in the cabin area of the wreckage. Also the closure mechanisms for several military type duffle bags were found and only two seats were installed in the cockpit. Examination of the engines revealed both to be operable at the time of the accident. The date and time of the accident could not be determined. The origin and destination of the flight could also not be determined. The aircraft was last seen at the Fort Lauderdale-Executive Airport on 2/3/86.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: maneuvering
Findings
1. (f) object - tree(s)
2. (c) preflight planning/preparation - inadequate - pilot in command
3. (c) in-flight planning/decision - improper - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
4. Terrain condition - high vegetation
Final Report: