Crash of a De Havilland L-20A Beaver in Lauterbach

Date & Time: Oct 14, 1958 at 0015 LT
Type of aircraft:
Operator:
Flight Phase:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While cruising by night in limited visibility due to fog, the single engine airplane crashed in a prairie located in Lauterbach, northwest of Fulda. Both occupants were injured while the aircraft was damaged beyond repair.

Crash of a Nord 2501D Noratlas in Böcklweiher: 6 killed

Date & Time: Jul 15, 1958
Type of aircraft:
Operator:
Registration:
AS+575
Flight Phase:
Flight Type:
Survivors:
No
MSN:
005
YOM:
1953
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The crew was performing a test flight when control was lost. The airplane crashed in unknown circumstances in Böcklweiher near Berchtesgaden. All six crew members were killed.

Crash of a Curtiss C-46F-1-CU Commando in Stuttgart

Date & Time: Jun 19, 1958
Type of aircraft:
Operator:
Registration:
LX-LAA
Flight Type:
Survivors:
Yes
Schedule:
Stuttgart - Stuttgart
MSN:
22422
YOM:
1945
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing a local training flight at Stuttgart-Echterdingen Airport. On touchdown, the left main gear collapsed. The airplane went out of control, veered off runway to the left and came to rest in flames. Both pilots were able to evacuate without injuries while the aircraft was destroyed by fire.
Probable cause:
Failure of the left main gear on touchdown.

Crash of an Airspeed AS.57 Ambassador 2 in Munich: 23 killed

Date & Time: Feb 6, 1958 at 1603 LT
Type of aircraft:
Operator:
Registration:
G-ALZU
Flight Phase:
Survivors:
Yes
Schedule:
Belgrade – Munich – Manchester
MSN:
5217
YOM:
1951
Flight number:
CY609
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
38
Pax fatalities:
Other fatalities:
Total fatalities:
23
Captain / Total flying hours:
7337
Captain / Total hours on type:
1722.00
Copilot / Total flying hours:
8463
Copilot / Total hours on type:
3143
Circumstances:
The aircraft had carried out a special flight on 3 February 1958, from England to Belgrade, making an intermediate landing at Munich-Riem Airport for refuelling purposes. On 6 February it flew back from Belgrade, bound for Manchester. As planned, it again made an intermediate landing at Munich to refuel, landing there at 1417LT. The aircraft made three attempts at take-off, two were abandoned, and the accident occurred during the third attempt. The copilot abandoned the first take-off because the boost pressure readings of both engines showed upward variations, rising 2 or 3 inches above the usual reading of 57.5 inches. The second attempt to take-off followed immediately after the aircraft had taxied back to the beginning of the runway. The engine run-up was not repeated. The captain abandoned the second take-off because the boost pressure reading (this time on the port engine only) again rose beyond the normal maximum value to 60 inches. In each case the take-off was abandoned approximately half way down the runway. After the second attempt the aircraft continued rolling as far as the end of the runway and from there proceeded to the terminal building. The passengers disembarked, and the BEA station engineer went aboard. He then pointed out to the two pilots that the variations in boost pressure were connected with the elevation of Munich Airport. After a short discussion, the pilots decided to make a third (attempt at) take-off, and the passengers were told to board the aircraft again. Before the fresh (attempt to) take- off, a further engine run-up was carried out. After take-off had begun, the boost pressure reading of the port engine again fluctuated somewhat, but this ceased after the captain had throttled back slightly for a short time. After he had opened up the throttle fully again, no further fluctuation were observed. The aircraft never became airborne in the course of the third attempt at take-off. It traveled on over the whole length of the runway and the adjoining grass-covered stopway (250 m). At the end of the stopway it crashed through a wooden fence which marked the aerodrome boundary, cleared a secondary road and struck a house standing on the other side of the road. The left wing was torn off outboard of the engine mounting. Parts of the tail unit were also torn off here. The house caught fire. The aircraft then crashed into a wooden hut standing on a concrete base about 100 m further on, striking it with the right side of the rear section of the fuselage. The fuselage was torn away on a level with the trailing edge of the wing. The hut and the part of the fuselage which was torn away caught fire. The remainder of the aircraft wreckage slid on for a further 70 m. Of the 44 occupants (6 crew and 38 passengers) on board, 21 were killed instantly. The others received injuries of a more or less serious nature. Two died later in hospital as a result of their injuries. The house which was struck by the aircraft was badly damaged by fire. The hut was destroyed by fire. Among those killed were eight players and the trainer. The president of the club and ten other players survived the accident.
Probable cause:
During the stop of almost two hours at Munich, a rough layer of ice formed on the upper surface of the wings as a result of snowfall. This layer of ice considerably impaired the aerodynamic efficiency of the aircraft, had a detrimental effect on the acceleration of the aircraft during the take-off process and increased the required unstick-speed. Thus, under the conditions obtaining at the time of take-off, the aircraft was not able to attain this speed within the rolling distance available. It is not out of the question that, in the final phase of the take-off process, further causes may also have had an effect on the accident. British tests on the effect of slush on the takeoff process of an aircraft led the Luftfahrt-Bundesamt to decide to re-open the investigation in November 1964. In August 1966 the Commission arrived at the view that in the runway conditions obtaining at Munich-Riem at the time of the accident, the aircraft G-ALZU without ice on the wing upper surfaces could have attained the required unstick-speed and would have been bound to have done so. The failure to unstick, and hence the accident, are thus to be attributed to a series of inter-related causal factors viz.:
- Decrease in the lift coefficient resulting from ice on the wing upper surfaces and a consequent increase in the minimum unstick speed,
- Increase in drag caused by ice accretion, particularly at the higher angle of incidence during the unstick process,
- Reduction by slush and spray of the margin of performance of the aircraft and effect of the slush on the trim.
The differing assessments of the situation by the two pilots during the final phase of the take-off to be inferred from Captain Thain's statements resulted in their acting in opposition which probably increased the severity of the accident.
Final Report:

Crash of a Douglas C-47A-5-DL at Wiesbaden AFB: 5 killed

Date & Time: Dec 17, 1957
Operator:
Registration:
42-23356
Flight Type:
Survivors:
Yes
MSN:
9218
YOM:
1943
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
On final approach to Wiesbaden-Erbenheim AFB, the twin engine aircraft struck the ground and crashed 4 km short of runway threshold. Five crew members were killed and a sixth was injured.

Crash of a Douglas C-54A-1-DO Skymaster in Düsseldorf: 7 killed

Date & Time: Nov 3, 1957 at 0703 LT
Type of aircraft:
Operator:
Registration:
D-ALAF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Düsseldorf – Reykjavik – New York
MSN:
7459
YOM:
1944
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The flight was to be from Dusseldorf, Germany, to New York via Reykjavik. One crew was to pilot the first leg of the trip to Reykjavik and the relief crew was to complete the flight to New York. Of the ten aboard the aircraft, seven were crew and three were passengers. Take-off from Dusseldorf at 0700 hours was normal until the aircraft became airborne. Immediately after becoming airborne and following retraction of the gear No. 1 engine was cut off and its propeller feathered. Then the No. 2 engine was also cut off and its propeller feathered. During this process the flaps were immediately and fully retracted. The aircraft, having attained an altitude of 50 metres, dropped sharply, lost altitude and crashed (0703 hours) into buildings within the city limits killing six of the occupants instantly and seriously injuring the other four. In addition, one person on the ground was killed and two others seriously injured. The wreckage was completely destroyed by fire.
Probable cause:
The accident was caused by the intentional creation of an emergency situation on take-off for a long distance flight: first No. 1 engine was cut off and its propeller feathered, then No. 2 engine was also stopped and its propeller feathered. In addition, the flaps were immediately and fully retracted at low altitude. Such action by the pilot-in-command during take-off immediately after the aircraft became airborne, with a view to testing a crew member, caused the aircraft to crash. The piloting technique was not consistent with the safety requirements and operating instructions as prescribed by the Directorate of Civil Aviation.
Final Report:

Crash of an Avro 652 Anson C.19 in Krefeld

Date & Time: Aug 21, 1957
Type of aircraft:
Operator:
Registration:
TX215
Flight Phase:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was forced to attempt an emergency landing following a fuel exhaustion. The twin engine aircraft crash landed in a field and came to rest. There were no injuries.
Probable cause:
Fuel exhaustion.

Crash of a De Havilland L-20A Beaver on Mt Hoher Ochsenkopf: 4 killed

Date & Time: May 21, 1957
Type of aircraft:
Operator:
Flight Phase:
Flight Type:
Survivors:
No
Site:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The aircraft lost height following the engine failure and crashed on the wooded Mt Hoher Ochsenkopf (1,054 meters high) located about 5 km west of Raumünzach. All four occupants were killed.

Crash of a Convair CV-340-58 in Munich: 3 killed

Date & Time: Dec 22, 1956 at 2103 LT
Type of aircraft:
Operator:
Registration:
YU-ADA
Survivors:
Yes
Schedule:
Belgrade – Vienna – Munich – Frankfurt – London
MSN:
162
YOM:
1954
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft was on a scheduled flight from Belgrade to Munich-Riem Airport with an intermediate refueling stop at Vienna. It departed from Vienna for Munich at 1837LT with 30 people aboard. At 2033, after passing Munich NDB at 12 000 feet, the flight reported to Munich Area Control Centre and shortly thereafter was instructed to descend to 10 000 feet. The pilot was asked whether he wished an ILS approach monitored by GCA but he decided on a GCA approach. At approximately 2048, after overflying non- directional beacon DHR (35 km east of Riem Airport), a further descent to 7 000 feet was carried out. A subsequent instruction to descend to 4 000 feet was also complied with and the pilot was asked to notify GCA when passing 6 000 feet. At 2053 the flight was cleared for a direct instrument approach to runway 25. At 2056 it reported passing 6 300 feet and at 2058 as having reached 3 500 feet. It was then cleared to descend to 3 000 this altitude was to be maintained. The flight was then 7 miles east of the airport. At 2059 the pilot reported leaving 3 000 feet and was requested to carry out the necessary cockpit checks for landing. GCA ordered a course of 240 degrees and advised the pilot that he was 4.5 miles from touchdown. He was requested to maintain 3 000 feet and was ordered to pull up to this altitude as he was below the minimum height of his glide path. No answer was received. The aircraft struck the ground at approximately 2103 hours, killing 2 crew members and 1 passenger and injuring 12 others.
Probable cause:
Considering the copilot's statement, the suddenly increased speed of descent could have been caused by the fact that the aircraft was pulled up to too great an extent which resulted in a subsequent dive. Even after a most thorough investigation of all reports, testimony and evidence, the Commission of Inquiry was not in a position to reach a final conclusion as to what caused the accident. The Commission is of the opinion that a further clarification would be possible if the surviving copilot, who is suffering from retrograde amnesia, could be questioned once more on certain points of his written declaration, in particular in regard to the question whether and how far piloting led to a fast let- down of the aircraft from which it could not be brought up again in time.
Final Report:

Crash of a Douglas C-47D at Fürstenfeldbruck AFB

Date & Time: Sep 13, 1956
Operator:
Registration:
44-77285
Flight Type:
Survivors:
Yes
MSN:
16869/33617
YOM:
1945
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach, the airplane crashed in unknown circumstances one km short of runway threshold. All nine occupants were evacuated safely while the aircraft was written off.