Country
Crash of an ATR72-600 in Semarang
Date & Time:
Dec 25, 2016 at 1824 LT
Registration:
PK-WGW
Survivors:
Yes
Schedule:
Bandung – Semarang
MSN:
1234
YOM:
2015
Flight number:
IW1896
Crew on board:
4
Crew fatalities:
Pax on board:
68
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
3805.00
Copilot / Total hours on type:
3200
Aircraft flight hours:
3485
Aircraft flight cycles:
4104
Circumstances:
On 25 December 2016, an ATR 72-600 aircraft registered PK-WGW was being operated by PT. Wings Abadi Airlines (Wings Air) as a scheduled passenger flight from Husein Sastranegara International Airport (WICC), Bandung to Ahmad Yani International Airport (WAHS), Semarang with flight number WON 1896. On board the aircraft were two pilots, two flight attendants and 68 passengers. There was no report or record of aircraft system malfunction prior to the departure. The aircraft departed from Bandung at 1734 LT (1034 UTC). The Pilot in Command (PIC) acted as Pilot Flying (PF) and the Second in Command (SIC) acted as Pilot Monitoring (PM). The flight from departure until commenced for landing approach was uneventful. At 1112 UTC, at night condition, the air traffic controller of Semarang Approach unit (approach controller) informed to all traffic that the rain was falling over the airport and the pilot confirmed whether the rain was heavy and was replied that it was slight rain. At 1115 UTC, the flight held over waypoint KENDA for separation with another aircraft and maintained altitude of 4,000 feet. Two minutes later, the flight was approved to descend to altitude of 3,000 feet. At 1118 UTC, the approach controller issued clearance for RNAV approach to runway 13 and advised the pilot to report when leaving waypoint KENDA. One minute later, the pilot reported leaving waypoint KENDA and the approach controller instructed to continue approach and to contact to the air traffic controller of Semarang Tower unit (tower controller). At 1120 UTC, the pilot advised to the tower controller that the aircraft was on final and the runway was in sight. The tower controller instructed to continue the landing approach and advised that the surface wind direction was 190° with velocity of 15 knots, altimeter setting 1,008 mbs and the runway was wet. At 1121 UTC, the tower controller had visual contact to the aircraft and issued landing clearance, the pilot read back the clearance and requested to reduce the approach light intensity. The tower controller reduced the light intensity and confirmed whether the intensity was appropriate then the pilot affirmed. At 1124 UTC, the aircraft touched down and bounced. After the third bounce, the pilot attempted to go around and the aircraft touched the runway. The tower controller noticed that the red light on the right wing was lower than the green light on the left wing. The aircraft moved to the right from the runway centerline and stopped near taxiway D. The tower controller realized that the aircraft was not in normal condition and pressed the crass bell then informed the Airport Rescue and Fire Fighting (ARFF) personnel by phone that there was aircraft accident near the taxiway D. At 1126 UTC, the pilot advised the tower controller that the aircraft stopped on the runway and requested assistance. The tower controller acknowledged the message and advised the pilot to wait for the assistance. While waiting the assistance, the pilot kept the engines run to provide lighting in the cabin. At 1129 UTC, the tower controller advised the pilot to shut down the engines since the ARFF personnel had arrived near the aircraft to assist the evacuation. Passenger evacuation completed at approximately 10 minutes after the aircraft stopped.
Probable cause:
Contributing Factors:
- The visual illusion of aircraft higher than the real altitude resulted in late flare out which made the aircraft bounced.
- The unrecovered bounce resulted in abnormal landing attitude with vertical acceleration up to 6 g and collapsed the right main landing gear.
- The visual illusion of aircraft higher than the real altitude resulted in late flare out which made the aircraft bounced.
- The unrecovered bounce resulted in abnormal landing attitude with vertical acceleration up to 6 g and collapsed the right main landing gear.
Final Report:
Crash of an ATR72-600 in Taipei: 43 killed
Date & Time:
Feb 4, 2015 at 1054 LT
Registration:
B-22816
Survivors:
Yes
Schedule:
Taipei - Kinmen
MSN:
1141
YOM:
2014
Flight number:
GE235
Crew on board:
5
Crew fatalities:
Pax on board:
53
Pax fatalities:
Other fatalities:
Total fatalities:
43
Captain / Total hours on type:
3151.00
Copilot / Total hours on type:
5687
Aircraft flight hours:
1627
Aircraft flight cycles:
2356
Circumstances:
The twin turboprop took off from runway 10 at 1052LT. While climbing to a height of 1,200 feet, the crew sent a mayday message, stating that an engine flamed out. Shortly later, the aircraft stalled and banked left up to an angle of 90° and hit the concrete barrier of a bridge crossing over the Keelung River. Out of control, the aircraft crashed into the river and was destroyed. It has been confirmed that 40 occupants were killed while 15 others were rescued. Three occupants remains missing. A taxi was hit on the bridge and its both occupants were also injured. According to the images available, it appears that the left engine was windmilling when the aircraft hit the bridge. First investigations reveals that the master warning activated during the initial climb when the left engine was throttled back. Shortly later, the right engine auto-feathered and the stall alarm sounded.
Probable cause:
The accident was the result of many contributing factors which culminated in a stall-induced loss of control. During the initial climb after takeoff, an intermittent discontinuity in engine number 2’s auto feather unit (AFU) may have caused the automatic take off power control system (ATPCS) sequence which resulted in the uncommanded autofeather of engine number 2 propellers. Following the uncommanded autofeather of engine number 2 propellers, the flight crew did not perform the documented abnormal and emergency procedures to identify the failure and implement the required corrective actions. This led the pilot flying (PF) to retard power of the operative engine number 1 and shut down it ultimately. The loss of thrust during the initial climb and inappropriate flight control inputs by the PF generated a series of stall warnings, including activation of the stick shaker and pusher. After the engine number 1 was shut down, the loss of power from both engines was not detected and corrected by the crew in time to restart engine number 1. The crew did not respond to the stall warnings in a timely and effective manner. The aircraft stalled and continued descent during the attempted engine restart. The remaining altitude and time to impact were not enough to successfully restart the engine and recover the aircraft.
The following findings related to probable causes were noted:
An intermittent signal discontinuity between the auto feather unit (AFU) number 2 and the torque sensor may have caused the automatic take off power control system (ATPCS):
- Not being armed steadily during takeoff roll,
- Being activated during initial climb which resulted in a complete ATPCS sequence including the engine number 2 autofeathering.
The available evidence indicated the intermittent discontinuity between torque sensor and auto feather unit (AFU) number 2 was probably caused by the compromised soldering joints inside the AFU number 2.
The flight crew did not reject the take off when the automatic take off power control system ARM pushbutton did not light during the initial stages of the take off roll.
TransAsia did not have a clear documented company policy with associated instructions, procedures, and notices to crew for ATR72-600 operations communicating the requirement to reject the take off if the automatic take off power control system did not arm.
Following the uncommanded autofeather of engine number 2, the flight crew failed to perform the documented failure identification procedure before executing any actions. That resulted in pilot flying’s confusion regarding the identification and nature of the actual propulsion system malfunction and he reduced power on the operative engine number 1.
The flight crew’s non-compliance with TransAsia Airways ATR72-600 standard operating procedures - Abnormal and Emergency Procedures for an engine flame out at take off resulted in the pilot flying reducing power on and then shutting down the wrong engine.
The loss of engine power during the initial climb and inappropriate flight control inputs by the pilot flying generated a series of stall warnings, including activation of the stick pusher. The crew did not respond to the stall warnings in a timely and effective manner.
The loss of power from both engines was not detected and corrected by the crew in time to restart an engine. The aircraft stalled during the attempted restart at an altitude from which the aircraft could not recover from loss of control.
Flight crew coordination, communication, and threat and error management (TEM) were less than effective, and compromised the safety of the flight. Both operating crew members failed to obtain relevant data from each other regarding the status of both engines at different points in the occurrence sequence. The pilot flying did not appropriately respond to or integrate input from the pilot monitoring.
The engine manufacturer attempted to control intermittent continuity failures of the auto feather unit (AFU) by introducing a recommended inspection service bulletin at 12,000 flight hours to address aging issues. The two AFU failures at 1,624 flight hours and 1,206 flight hours show that causes of intermittent continuity failures of the AFU were not only related to aging but also to other previously undiscovered issues and that the inspection service bulletin implemented by the engine manufacturer to address this issue before the occurrence was not sufficiently effective. The engine manufacturer has issued a modification addressing the specific finding of this investigation. This new modification is currently implemented in all new production engines, and another service bulletin is available for retrofit.
Pilot flying’s decision to disconnect the autopilot shortly after the first master warning increased the pilot flying’s subsequent workload and reduced his capacity to assess and cope with the emergency situation.
The omission of the required pre-take off briefing meant that the crew were not as mentally prepared as they could have been for the propulsion system malfunction they encountered after takeoff.
The following findings related to probable causes were noted:
An intermittent signal discontinuity between the auto feather unit (AFU) number 2 and the torque sensor may have caused the automatic take off power control system (ATPCS):
- Not being armed steadily during takeoff roll,
- Being activated during initial climb which resulted in a complete ATPCS sequence including the engine number 2 autofeathering.
The available evidence indicated the intermittent discontinuity between torque sensor and auto feather unit (AFU) number 2 was probably caused by the compromised soldering joints inside the AFU number 2.
The flight crew did not reject the take off when the automatic take off power control system ARM pushbutton did not light during the initial stages of the take off roll.
TransAsia did not have a clear documented company policy with associated instructions, procedures, and notices to crew for ATR72-600 operations communicating the requirement to reject the take off if the automatic take off power control system did not arm.
Following the uncommanded autofeather of engine number 2, the flight crew failed to perform the documented failure identification procedure before executing any actions. That resulted in pilot flying’s confusion regarding the identification and nature of the actual propulsion system malfunction and he reduced power on the operative engine number 1.
The flight crew’s non-compliance with TransAsia Airways ATR72-600 standard operating procedures - Abnormal and Emergency Procedures for an engine flame out at take off resulted in the pilot flying reducing power on and then shutting down the wrong engine.
The loss of engine power during the initial climb and inappropriate flight control inputs by the pilot flying generated a series of stall warnings, including activation of the stick pusher. The crew did not respond to the stall warnings in a timely and effective manner.
The loss of power from both engines was not detected and corrected by the crew in time to restart an engine. The aircraft stalled during the attempted restart at an altitude from which the aircraft could not recover from loss of control.
Flight crew coordination, communication, and threat and error management (TEM) were less than effective, and compromised the safety of the flight. Both operating crew members failed to obtain relevant data from each other regarding the status of both engines at different points in the occurrence sequence. The pilot flying did not appropriately respond to or integrate input from the pilot monitoring.
The engine manufacturer attempted to control intermittent continuity failures of the auto feather unit (AFU) by introducing a recommended inspection service bulletin at 12,000 flight hours to address aging issues. The two AFU failures at 1,624 flight hours and 1,206 flight hours show that causes of intermittent continuity failures of the AFU were not only related to aging but also to other previously undiscovered issues and that the inspection service bulletin implemented by the engine manufacturer to address this issue before the occurrence was not sufficiently effective. The engine manufacturer has issued a modification addressing the specific finding of this investigation. This new modification is currently implemented in all new production engines, and another service bulletin is available for retrofit.
Pilot flying’s decision to disconnect the autopilot shortly after the first master warning increased the pilot flying’s subsequent workload and reduced his capacity to assess and cope with the emergency situation.
The omission of the required pre-take off briefing meant that the crew were not as mentally prepared as they could have been for the propulsion system malfunction they encountered after takeoff.
Final Report: